Abstract
The casting of precision components for high-speed railway brake systems has garnered significant attention due to their enhanced machinability, shock absorption, and cost-effectiveness. The brake unit box, a critical support structure in high-speed railway braking systems, is particularly critical in ensuring the safety and performance of trains. This paper presents a comprehensive numerical simulation and process optimization study for the casting of a high-speed railway brake unit box. The AnyCasting software was employed to analyze the filling, solidification, and shrinkage processes, revealing potential defects such as shrinkage porosity and hot tears. Based on the simulation results, several process improvements were proposed, including modifying the gating system, incorporating heated risers, and optimizing the feeding channels. The effectiveness of these modifications was verified through additional numerical simulations and experimental casting trials. The results demonstrated that the optimized casting process resulted in a defect-free brake unit box with mechanical properties that met the design specifications.

1. Introduction
High-speed railway brake unit boxes play a pivotal role in ensuring the safety and reliability of high-speed trains. These boxes are subject to complex loading conditions and must withstand high dynamic forces during braking. Therefore, they require exceptional mechanical properties and dimensional accuracy. Traditional casting processes often encounter challenges in achieving the desired quality due to the intricate geometry and thin walls of the brake unit box.
Numerical simulation tools offer a powerful means of predicting and mitigating casting defects during the design and production phases. In this study, we employed the AnyCasting software to simulate the casting process of a high-speed railway brake unit box. Based on the simulation results, we optimized the gating system, incorporated heated risers, and modified the feeding channels to ensure defect-free castings.
2. Material and Methods
2.1 Box Geometry and Design Specifications
The brake unit box considered in this study has a complex geometry with multiple internal cavities and thin walls. The box dimensions are 302 mm x 287 mm x 235 mm, and it weighs approximately 14 kg. The box is designed to withstand high mechanical loads and must be free from defects such as porosity, hot tears, and inclusions.
2.2 Material Properties
The brake unit box was cast using a gray iron alloy with the following chemical composition:
- Carbon (C): 3.6% to 3.7%
- Silicon (Si): 2.55% to 2.65%
- Manganese (Mn): 0.65% to 0.75%
- Phosphorus (P): ≤ 0.02%
- Sulfur (S): ≤ 0.015%
- Copper (Cu): 0.3% to 0.4%
- Magnesium (Mg): 0.035% to 0.05%
2.3 Numerical Simulation Software
The AnyCasting software was used to simulate the casting, solidification, and shrinkage processes. This software enables the prediction of filling velocity, temperature distribution, and defect formation within the casting. The simulation parameters were set according to the material properties and casting conditions, as summarized in Table 1.
Table 1: Simulation Parameters
Parameter | Value |
---|---|
Pouring temperature | 1400°C |
Mold temperature | 200°C |
Chemical composition | As specified |
Gate diameter | 50 mm |
Riser diameter | 75 mm (main), 60 mm (flange) |
Riser height | 90 mm |
Pouring time per mold | 9 s |
3. Initial Simulation Results
3.1 Filling Process
The initial simulation results revealed potential issues during the filling process. the metal flow entered the mold cavity at a high velocity, leading to turbulence and a risk of erosion. The overall filling pattern exhibited turbulent flow, with localized high-velocity regions. Despite the high filling temperature, the turbulent flow increased the risk of entrapped air and oxides.
3.2 Solidification and Shrinkage
The solidification simulation identified three significant isolated liquid regions, indicating potential shrinkage porosity. The probability of defect formation was high (above 60%) in five locations, primarily in the thicker sections of the box.
4. Process Optimization
Based on the initial simulation results, several process improvements were proposed to mitigate the identified defects.
4.1 Modified Gating System
The gating system was redesigned to reduce turbulence and improve metal flow control. A new gate configuration with reduced cross-sectional areas was implemented. This modification aimed to slow down the initial metal flow and ensure a smoother, more controlled filling pattern.
4.2 Incorporation of Heated Risers
Heated risers (FT500-M50x75 model from Shengquan Group) were incorporated to enhance feeding and promote directional solidification. The heated risers maintained a consistent temperature during the casting process, ensuring adequate metal supply to the critical sections during solidification.
4.3 Optimization of Feeding Channels
Additional feeding channels were introduced to connect the main riser to the flange risers, enhancing the feeding efficiency and reducing the risk of shrinkage porosity. These channels were designed based on the defect probability map from the initial simulation.
5. Verification through Simulation and Experiments
5.1 Simulation Verification
The optimized process was verified through additional AnyCasting simulations. The results indicated significant improvements in the filling and solidification processes. the metal flow was smoother, with reduced turbulence and erosion risks. The filling temperature remained above the solidus line throughout the process, minimizing the risk of cold shuts. The oxide formation was negligible.
The solidification simulation demonstrated improved directional solidification and the elimination of isolated liquid regions. The defect probability was significantly reduced, with no defects predicted in the critical box sections.
5.2 Experimental Verification
Experimental castings were produced using the optimized process. The castings were sectioned and subjected to dye penetrant inspection to detect any internal defects. The results confirmed the absence of shrinkage porosity, hot tears, or inclusions.
6. Mechanical Properties and Microstructure
The experimental castings were further analyzed for mechanical properties and microstructure. The tensile strength, yield strength, elongation, and hardness were measured and compared with the customer specifications (Table 2). The balling rate and pearlite content were also evaluated to assess the microstructure quality.
Table 2: Mechanical Properties of Experimental Castings
Property | Specification | Measured Value |
---|---|---|
Tensile strength (MPa) | ≥ 500 | 566 |
Yield strength (MPa) | ≥ 320 | 368 |
Elongation (%) | ≥ 7 | 14 |
Hardness (HBW) | 70-230 | 198 |
Balling rate (%) | N/A | 85 |
Pearlite content (%) | N/A | 45 |
The microstructure analysis revealed a well-developed pearlitic matrix with a balling rate of 85%. The microstructure was free from graphite nodules or flocculent graphite, indicating proper solidification conditions.
7. Conclusion
This study demonstrated the effectiveness of numerical simulation in optimizing the casting process for a high-speed railway brake unit box. Through the AnyCasting software, potential defects such as shrinkage porosity and hot tears were identified in the initial casting design. Based on these findings, several process improvements were proposed and verified through additional simulations and experimental castings.
The optimized process resulted in defect-free castings with mechanical properties that exceeded the customer specifications. The use of heated risers and optimized feeding channels promoted directional solidification and minimized shrinkage porosity. The experimental results confirmed the effectiveness of the optimized process, demonstrating the potential of numerical simulation in enhancing casting quality and reducing production costs.