In modern engine cylinder block production, machining defects such as tool marks on critical surfaces like the #399 cylinder head joint face significantly impact manufacturing efficiency and product quality. This study investigates root causes and implements optimization measures to reduce rework rates and tooling costs.
Problem Analysis
The engine cylinder block manufacturing process exhibited excessive tool mark defects (15.25% tool return rate) and monthly scrap exceeding 337 units. Key defect characteristics included:
- Surface roughness exceeding Ra 1.6 μm
- Parallelism deviation > 0.05 mm
- Visual tool path patterns on #399 surface

Root Cause Identification
Using fishbone analysis, 10 potential factors were identified and verified through experimental testing:
Factor | Test Method | Impact Level |
---|---|---|
Tool height variation | Height difference measurement | High (83% defect correlation) |
Cutting path strategy | Path simulation | Medium |
Tool life management | Wear pattern analysis | High |
Key Parameter Optimization
The cutting force model for engine cylinder block machining can be expressed as:
$$ F = K_c \times a_p \times f \times \cos{\alpha} $$
Where:
$F$ = Cutting force (N)
$K_c$ = Specific cutting force (N/mm²)
$a_p$ = Depth of cut (mm)
$f$ = Feed rate (mm/rev)
$\alpha$ = Tool approach angle
Tool life optimization followed Taylor’s equation:
$$ VT^n = C $$
Where:
$V$ = Cutting speed (m/min)
$T$ = Tool life (min)
$n,C$ = Material constants
Implementation Results
Optimization measures achieved significant improvements in engine cylinder block machining:
Parameter | Before | After |
---|---|---|
Tool mark return rate | 15.25% | 5.88% |
Surface roughness (Ra) | 2.1 μm | 1.2 μm |
Tool life (pieces/edge) | 220 | 300 |
Process Improvements
Critical modifications for engine cylinder block machining included:
- Tool Height Control: Reduced active cutting edges from 3 to 1
$$ \Delta h = |h_1 – h_2| \leq 5\,\mu m $$ - Cutting Path Revision: Implemented bidirectional milling
$$ L_{path} = 2 \times (L_{block} + W_{block}) $$ - Tool Life Adjustment: Optimized replacement frequency
$$ N_{opt} = \sqrt{\frac{C_t}{C_m}} $$
Where $C_t$ = Tool cost, $C_m$ = Machine hour rate
Conclusion
Through systematic analysis and parameter optimization, the engine cylinder block manufacturing process achieved 61.4% reduction in tool mark defects. The implemented solutions demonstrate effective quality control strategies for complex machining operations in engine component production.