This paper presents a comprehensive investigation of casting defects in thin-walled sections of complex nodular iron castings, focusing on shrinkage porosity in intake/exhaust ports and slag inclusion at spring seat surfaces of marine diesel cylinder heads. Through systematic process optimization, defect rates were reduced from 50% to 93% in actual production.
1. Material Characteristics and Defect Formation
The cylinder head material QT400-15 exhibits typical nodular iron properties with the chemical composition shown in Table 1. The characteristic “mushy” solidification behavior of nodular iron can be expressed as:
$$ \frac{dV}{dt} = \alpha(T) \cdot (V_{graphite} – V_{matrix}) $$
where α(T) represents the temperature-dependent expansion coefficient, and V denotes volume fractions of different phases.

Element | C | Si | Mn | P | S | Mg |
---|---|---|---|---|---|---|
Content | 3.2-3.8 | 2.4-3.3 | <0.35 | <0.07 | <0.02 | 0.03-0.10 |
2. Thin-Wall Shrinkage Porosity Mechanism
For thin-wall sections (8-10mm), the critical solidification time can be calculated using:
$$ t_c = \left(\frac{\delta}{2k}\right)^2 $$
where δ = wall thickness, k = solidification constant (0.8-1.2 cm/min½ for nodular iron). When localized thermal gradients exceed 15°C/cm, isolated hot spots form, leading to casting defects.
3. Process Optimization Strategies
Key improvements for casting defect elimination include:
3.1 Chill Optimization
The modified chill layout achieved uniform cooling through:
$$ Q_{chill} = \rho \cdot c_p \cdot V_{chill} \cdot \Delta T $$
where ρ = 7.8 g/cm³, cp = 0.46 kJ/kg·K, and ΔT = 1150°C. Chill coverage increased from 42% to 98% of critical surfaces.
Parameter | Original | Optimized |
---|---|---|
Chill Coverage (%) | 42 | 98 |
Machining Allowance (mm) | 3 | 8 |
Pouring Temperature (°C) | 1420 | 1390 |
3.2 Slag Control Mechanism
The modified gating system enhanced slag flotation through velocity control:
$$ v_{max} = \sqrt{\frac{2g(h + p/\rho)}{1 + fL/D}} $$
where h = metallostatic head, p = atmospheric pressure, f = friction factor. Increased machining allowance (3→8mm) provided sufficient safety margin for complete slag removal.
4. Quality Improvement Results
The implemented solutions demonstrated significant casting defect reduction:
$$ \eta = \frac{N_{defect-free}}{N_{total}} \times 100\% = \frac{121}{130} \times 100\% = 93\% $$
Key performance indicators showed:
- Shrinkage porosity occurrence decreased by 87%
- Slag inclusion rates reduced by 95%
- Dimensional accuracy improved to CT8 grade
5. Thermal Analysis Verification
Numerical simulation confirmed the elimination of isolated hot spots:
$$ \nabla \cdot (k\nabla T) = \rho c_p \frac{\partial T}{\partial t} $$
Post-optimization thermal profiles showed maximum temperature differentials reduced from 280°C to 85°C in critical sections, effectively preventing casting defect formation.
6. Production Validation
Field testing of 130 optimized castings demonstrated:
Test Parameter | Result |
---|---|
Pressure Test (25MPa) | 100% Pass |
Fatigue Cycles | >1×10⁷ |
Surface Roughness (Ra) | 3.2-6.3μm |
This systematic approach to casting defect control provides a reliable solution framework for complex thin-wall nodular iron components in marine applications.