Design and Optimization of Precision Investment Casting Process for Lifting Arm

Precision investment casting is widely employed for manufacturing complex components like industrial lifting arms due to its ability to produce high-dimensional accuracy and surface finish. This study focuses on optimizing the casting process of a ZG0Cr18Ni9Ti stainless steel lifting arm with dimensions 70 mm × 45 mm × 57 mm and average wall thickness of 6 mm, addressing shrinkage defects through systematic numerical analysis and experimental validation.

1. Structural Analysis and Initial Process Design

The lifting arm consists of three functional sections: U-shaped working claws, threaded connection holes, and stepped shafts. The initial gating system design followed a top-pouring configuration with one sprue, six runners, and six in-gates arranged symmetrically. The 3D finite element model containing 34,928 nodes and 249,485 elements was established using ProCAST software.

Element C Mn Si Cr Ni Ti P S
Content (%) ≤0.08 0.8-2.0 ≤1.5 17.0-20.0 8.0-11.0 0.3-0.7 ≤0.045 ≤0.030

The critical process parameters for precision investment casting were calculated using the Kargin formula:

$$ v = \frac{h}{\delta \sqrt{T}} $$

where \( v \) = pouring speed (cm/s), \( h \) = casting height (cm), \( δ \) = wall thickness (cm), and \( T \) = pouring temperature (°C). Initial parameters included:

  • Shell preheating temperature: 1,000°C
  • Pouring temperature: 1,530°C
  • Pouring speed: 350 mm/s

2. Numerical Simulation and Defect Analysis

ProCAST simulations revealed significant shrinkage porosity (>10% volumetric fraction) at junctions between stepped shafts and U-claws. The solidification sequence analysis showed premature freezing at structural intersections, blocking liquid metal feeding paths. Initial process results indicated:

Parameter Filling Time Solidification Time Shrinkage Rate
Value 3.9 s 778 s 12.45%

3. Gating System Optimization

Two modified designs were proposed for precision investment casting improvement:

  1. Scheme A: Added exhaust vents at thermal junctions
  2. Scheme B: Implemented supplementary feeders and enlarged runner diameters

Comparative simulation results demonstrated:

Scheme Shrinkage Rate Improvement
Initial 12.45%
A 10.21% 18.0%
B 2.92% 76.5%

4. Process Parameter Optimization

An orthogonal experiment (L9 array) evaluated three critical factors in precision investment casting:

Level A: Pouring Temp. (°C) B: Pouring Speed (mm/s) C: Shell Preheat (°C)
1 1,500 350 1,000
2 1,530 450 1,050
3 1,550 550 1,100

The shrinkage rate (\( S_r \)) was calculated using:

$$ S_r = \sum_{i=1}^{n} (V_{porosity_i}/V_{casting}) × 100\% $$

Experimental results and range analysis revealed:

Test A B C \( S_r \)
L1 1 1 1 1.25%
L2 1 2 2 1.15%
L3 1 3 3 1.32%
L4 2 1 2 1.26%
L5 2 2 3 1.29%
L6 2 3 1 1.23%
L7 3 1 3 1.32%
L8 3 2 1 1.28%
L9 3 3 2 1.28%

Range analysis determined optimal parameters as A1B2C2:

  • Shell preheating: 1,050°C
  • Pouring temperature: 1,500°C
  • Pouring speed: 450 mm/s

5. Validation and Industrial Application

The optimized precision investment casting process reduced shrinkage defects by 89.7% compared with initial conditions. Production trials confirmed:

Metric Initial Optimized
Defect Rate 15.2% 1.6%
Yield Improvement 32.5%
Cycle Time 45 min 38 min

This systematic approach demonstrates the effectiveness of combining numerical simulation with orthogonal experiments in precision investment casting optimization, providing valuable insights for complex thin-walled component manufacturing.

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