In my role as a casting engineer, I was tasked with developing a long-guide machine tool bed casting for a European client. This machine tool casting presented significant challenges due to its length of 4.5 meters, weight of 7.5 tons, and high precision requirements for both casting and machining. The material specified was EN-GJL-300, equivalent to HT300, with a single-cast tensile strength of at least 300 MPa, a hardness range of 200 HB to 230 HB, a pearlite content of over 98% in the matrix, and a dimensional tolerance of CT10 grade. The guide rail area demanded freedom from defects such as slag inclusions, sand inclusions, and shrinkage porosity. Given the high performance requirements and susceptibility to bending deformation, I embarked on a technical攻关 to optimize the process for this machine tool casting.
The development of machine tool castings like this one requires meticulous attention to structural integrity and process control. My approach involved a comprehensive analysis of the casting’s structure, followed by the design of key工艺 parameters, simulation using MAGMA software, and careful熔炼 and pouring practices. Throughout this project, I focused on ensuring that the final machine tool castings met all client specifications while minimizing defects and costs. The use of wood patterns and new iron sand boxes was adopted to balance quality and affordability for small-batch production.
Structural analysis revealed that the machine tool casting had wall thicknesses ranging from 20 mm to 50 mm, classifying it as a medium-thick-walled casting. The 4.5-meter guide rail was particularly prone to bending deformation, with the guide rail itself reaching a thickness of 115 mm. To ensure the quality of the guide rail surface, I decided to position it in the lower mold. This placement helped reduce deformation and maintain dimensional accuracy. The complex shape and lack of existing工艺装备 necessitated the use of wooden patterns and iron sand boxes, which I selected to achieve cost-effectiveness without compromising on the quality of the machine tool castings.

For the工艺 design, I began by determining the parting surface and basic parameters. The parting surface was established at the large cross-section to facilitate mold release and simplify operations, with most of the machine tool casting located in the lower box to minimize deformation. A resin sand process was employed for molding, with a casting shrinkage rate of 0.8% to 1%—1% in the length direction and 0.8% in the width direction. Machining allowances were set at 10 mm to 12 mm, and a reverse deformation amount of 3 mm was incorporated at the center guide rail to counteract potential bending. To ensure dimensional precision, I applied a core shift allowance of 0.5 mm for each sand core and a parting line allowance of 1 mm on both upper and lower surfaces to prevent metal leakage.
The sand core design was critical for this machine tool casting, as the guide rail faced downward, eliminating the use of core prints for positioning. Instead, I relied on core supports (chills) to hold the cores in place. The internal cavities were formed using furan resin sand cores, with core parting surfaces aligned with the mold parting surfaces to ensure uniform wall thickness and reduce flash. Cores were designed with vertical prints based on standard casting manuals, and loose pieces were used where ejection was restricted. The core supports were designed to withstand the weight of the cores and ensure proper fusion with the metal; several types were developed based on the core configurations, as summarized in the table below.
| Core Support Type | Dimensions (mm) | Application Area | 
|---|---|---|
| Type 1 | 14×20×25 with 1.5 mm fillet | Light-weight cores | 
| Type 2 | 19×30×24 with 3 mm thickness | Medium-weight cores | 
| Type 3 | 37×40 with 15° angle | Heavy-duty cores | 
| Type 4 | Ø35×21 | Circular support areas | 
The gating and feeding systems were designed to ensure smooth metal flow and effective feeding for the machine tool castings. The gating system introduced molten metal from both ends of the guide rail, supplemented by multiple ingates at other planar locations. A ceramic filter was incorporated to trap slag. The pouring time was calculated using the formula:
$$ t = S \frac{\sqrt{G}}{\delta} $$
where \( S \) is a coefficient (1.8 for quick pouring of large cast iron castings), \( G \) is the total pouring weight (7500 kg), and \( \delta \) is the average wall thickness (25 mm). This resulted in a pouring time of approximately 103 seconds. The choke area was determined by:
$$ F_{\text{choke}} = \frac{G}{0.31 \mu t \sqrt{H}} $$
where \( \mu \) is the flow loss coefficient (assumed 0.6 for resin sand), and \( H \) is the head height (measured as 50 cm). After calculations, the choke area was set to 64 cm², with an open gating system ratio of 1:1.2:1.4 for the cross-sectional areas.
For the feeding system, I identified 15 hot spots at cross-rib intersections that required risers. Given the gray iron material, which benefits from graphitization expansion for self-feeding, the risers were designed to supplement any insufficient feeding. Using the modulus method, I calculated riser dimensions: diameter of 150 mm, height of 250 mm, and neck dimensions of 80 mm diameter and 60 mm height. Additionally, vent channels were added at the top protrusions to facilitate gas escape, with a total cross-sectional area exceeding that of the sprue to prevent gas-related defects.
To validate the工艺, I conducted solidification simulations using MAGMA software. The filling simulation showed that metal entered the mold through the sprue, flowed along the runner to the ingates, and filled the cavity layer by layer without splashing or cold shuts. The total filling time was 112 seconds, confirming no issues like misruns. The solidification simulation indicated near-simultaneous solidification, with the guide rail and reinforcement ribs solidifying first, and the risers effectively feeding the last solidifying sections, minimizing shrinkage risks in the machine tool castings.
| Element | Target Range (Before Treatment) | Target Range (After Treatment) | 
|---|---|---|
| C | 2.9–3.1 | 2.9–3.1 | 
| Si | 1.3–1.5 | 1.7–1.9 | 
| Mn | 0.6–0.8 | 0.6–0.8 | 
| P | <0.05 | <0.05 | 
| S | 0.05–0.08 | 0.05–0.08 | 
| Cu | 0.15 | 0.7–1.0 | 
| Sn | — | 0.05–0.07 | 
In the melting and pouring phase, I controlled the chemical composition to achieve the desired properties for the machine tool castings. A 10-ton induction furnace was used, with a charge consisting of high proportions of steel scrap and returns, plus 10–15% pig iron. The carbon equivalent (CE) was maintained between 3.45% and 3.7% to reduce shrinkage. Manganese was kept at 0.6–0.8% to stabilize pearlite without harming graphite formation. Copper and tin were added as alloying elements to enhance strength, as allowed by the client. The composition was verified using spectroscopy and carbon-silicon analysis at 1450°C, and adjustments were made before heating to 1500°C and holding for 10–15 minutes.
Pouring was carried out at 1360–1380°C using a 10-ton ladle. Inoculation was performed with 2–5 mm strontium-silicon inoculant during tapping, followed by a second instant inoculation with 0.1–0.15% barium-silicon inoculant during pouring. This treatment improved the microstructure and mechanical properties of the machine tool castings, as evidenced by the test results below.
| Sample Type | Tensile Strength (MPa) | Hardness (HB) | Pearlite Content (%) | 
|---|---|---|---|
| Separately Cast Specimen | 335 | 205–209 (reference) | >98 | 
| Body Hardness | — | 207–225 | >98 | 
Production application confirmed the success of this工艺 for machine tool castings. The first casting underwent magnetic particle and penetrant testing, revealing no defects. Mechanical properties and microstructure met standards, with only a minor deformation of less than 5 mm at the bed center, within the machining allowance. This machine tool casting has since been approved for batch production, passing all European client inspections. My experience highlights the importance of integrated design, simulation, and controlled melting in producing high-quality machine tool castings for demanding applications.
Throughout this project, I refined my approach to handling large machine tool castings, emphasizing the need for precise core support design and optimized gating. The use of MAGMA simulation proved invaluable in predicting and mitigating defects, ensuring that the machine tool castings achieved the required performance. Future work could explore alternative alloying elements or advanced simulation techniques to further enhance the efficiency and quality of machine tool castings in industrial settings.
