In the development of advanced equipment, the production of large-scale structural components through steel casting processes presents significant challenges. This study focuses on the design and optimization of the casting process for a critical steel casting guide rail, which is integral to the performance and reliability of the equipment. As a researcher involved in this project, I aim to share a comprehensive account of our approach, from initial design to final validation, emphasizing the use of simulation tools and practical refinements to achieve high-quality steel castings. The steel casting industry continually seeks methods to improve the integrity and precision of large frame components, and this work contributes to that endeavor by addressing common defects such as misruns, cold laps, shrinkage, and deformation.
The guide rail in question is a large frame steel casting characterized by its complex geometry and stringent performance requirements. Its structure resembles a flattened,镂空 framework with interconnected ribs, measuring approximately 1596 mm in length, 501 mm in width, and 444 mm in height. The wall thickness varies significantly, ranging from 18 mm to 51 mm, which complicates the solidification and feeding dynamics during the steel casting process. Technically, the rail must exhibit no defects on its functional surfaces to ensure machining accuracy and withstand substantial impact and fatigue loads in service. These demands necessitate a robust casting methodology, as welding or other fabrication techniques would compromise the homogeneity and strength required. The primary difficulties in producing this steel casting include ensuring complete mold filling due to the long and tortuous flow paths, controlling dimensional accuracy amid complex contractions, and preventing internal defects like shrinkage porosity in thick sections.
To tackle these challenges, our team embarked on a systematic design of the steel casting process. We began by determining the optimal pouring position and parting plane. Given the component’s planar nature, we oriented the large flat surface horizontally for pouring, placing the entire casting in the drag mold. This orientation facilitates sequential solidification and minimizes misalignment risks. The parting surface was aligned with the pouring position to simplify patternmaking and molding operations, reducing the number of cores needed and enhancing inspection efficiency during assembly. This decision is crucial for large frame steel castings where precision is paramount.
The gating system was designed to accommodate the characteristics of steel casting, which involves high pouring temperatures and relatively low fluidity. We employed an open gating system with a bottom-pour ladle to achieve rapid filling and minimize turbulence. The cross-sectional areas were calculated based on the ladle nozzle area, denoted as \(F_{\text{nozzle}}\). For a nozzle diameter of 45 mm, the area is \(F_{\text{nozzle}} = 15.9 \, \text{cm}^2\). The subsequent elements were sized according to the ratios: \(F_{\text{nozzle}} : F_{\text{spure}} : F_{\text{runner}} : F_{\text{ingate}} = 1 : 1.8-2.0 : 1.8-2.0 : 2.0-2.5\). Thus, we derived: \(F_{\text{spure}} = 2.0 \times 15.9 = 31.8 \, \text{cm}^2\), corresponding to a 60 mm diameter spure; \(F_{\text{runner}} = 31.8 \, \text{cm}^2\), arranged in a stepped configuration to trap slag; and \(F_{\text{ingate}} = 2.5 \times 15.9 = 39.8 \, \text{cm}^2\), with flat, wide ingates attached to risers to promote smooth metal entry. The pouring time was estimated using the formula: $$t = \frac{G_L}{N \cdot n \cdot q}$$ where \(G_L = 330 \, \text{kg}\) is the weight of molten steel, \(N = 1\) (number of ladles), \(n = 1\) (number of nozzles), and \(q = 30 \, \text{kg/s}\) (average pouring rate). This yielded \(t \approx 11 \, \text{s}\), and we aimed for 10-14 s in practice.
Riser design is critical for feeding steel castings to prevent shrinkage defects. We applied the modulus method, where the modulus \(M\) is defined as the ratio of volume to cooling surface area: $$M = \frac{V}{A}$$ This principle states that regions with similar moduli solidify simultaneously. For the guide rail, we computed moduli for key sections to identify hot spots requiring risers. The results are summarized in Table 1, indicating that the overall modulus is relatively uniform, suggesting a near-simultaneous solidification pattern. Consequently, we positioned risers to create localized sequential solidification, using both side and top risers based on empirical knowledge.
| Section | Volume (cm³) | Surface Area (cm²) | Modulus (cm) |
|---|---|---|---|
| Overall Casting | 26,904.60 | 24,299.62 | 1.11 |
| Region 1 (Thin Wall) | 308.57 | 275.00 | 1.12 |
| Region 2 (Thick Junction) | 1,903.57 | 1,181.05 | 1.62 |
| Region 3 (Rib Intersection) | 1,294.63 | 786.02 | 1.65 |
| Region 4 (Edge Section) | 417.88 | 473.31 | 1.00 |
The pouring temperature was selected based on the material properties of ZG32MnMo steel, a low-alloy steel commonly used in heavy-duty steel castings. Its liquidus and solidus temperatures are 1503°C and 1448°C, respectively. To ensure proper fluidity while avoiding excessive thermal stress, we set the pouring temperature range at 1580–1600°C for the bottom-pour ladle operation. Controlling shrinkage is another vital aspect of steel casting process design. Due to the complex geometry and varying wall thicknesses, we assigned differential shrinkage allowances: 1.8% for length and width directions in internal cavities, and 2.0% for the height direction. This approach accounts for restraint from cores and uneven cooling, which are typical in large frame steel castings.
Initial trials were conducted using the designed steel casting process. We manufactured metal patterns and core boxes, utilizing dedicated flasks sized 1920 mm × 670 mm × 350/400 mm. The molding medium was “Bondi” resin sand, hand-molded and coated with zircon-based alcohol paint to improve surface finish. The steel was melted in a 3-ton basic electric arc furnace and poured via a 5-ton bottom-pour ladle. Four castings were produced to evaluate the process. Upon inspection, several defects were identified: misruns and cold laps on the upper surface edges and center; shrinkage cavities in side plates and ends of the rail surface; hot tears at sharp corners of connecting ribs; dimensional overshoot in internal length; and upward warping deformation at the four corners of the rail surface. These issues highlighted the inadequacies of the initial steel casting process.
Analysis revealed that the misruns and cold laps resulted from extensive heat loss during metal flow through intricate channels, a common problem in large steel castings with thin sections. Shrinkage cavities were attributed to inadequate feeding from dispersed small risers. Hot tears formed due to stress concentration at sharp corners where solidification contraction was restrained by the mold. Dimensional inaccuracies stemmed from incorrect shrinkage allowances and core restraint. The warping deformation was caused by tensile stresses from riser solidification, as the risers, located in the cope mold, pulled the corners upward during cooling. This understanding prompted us to refine the steel casting process using advanced simulation.
We employed ProCAST, a three-dimensional digital simulation software, to model the solidification and stress development in the steel casting. The simulation provided insights into temperature gradients, liquid fraction, and stress distribution. For instance, the effective stress analysis showed peak stresses of up to 251 MPa at certain fillets, but comparison with the temperature-dependent yield strength of ZG32MnMo (Figure 9) confirmed that this remained below critical levels. The yield strength of this steel casting material can be expressed as a function of temperature: $$\sigma_y(T) = \sigma_0 – k(T – T_0)$$ where \(\sigma_0\) is the yield strength at room temperature, \(k\) is a material constant, and \(T\) is the temperature. Simulation results indicated that stress concentrations were manageable, but deformation patterns necessitated adjustments.

Based on the simulation, we implemented several improvements to the steel casting process. First, we relocated the gating system from the periphery to the interior of the casting, with ingates feeding both side and central risers. This reduced flow distance and heat loss, enhancing mold filling. Additionally, we practiced post-pouring replenishment to counter misruns. Second, we replaced dispersed small risers with a consolidated larger riser system to improve feeding efficiency and reduce localized stresses. To combat warping, we added tying ribs between risers and incorporated a 4 mm reverse camber at the bottom corners, effectively offsetting anticipated deformation. The revised steel casting process layout is illustrated in Figure 11. Third, for dimensional control, we adjusted the shrinkage allowance for internal length to 1.5%, based on actual measurements from trial casts. During heat treatment, we altered the placement of steel castings from horizontal to vertical orientation, using welded reinforcements to prevent distortion, as shown in Figure 12. Lastly, to eliminate hot tears, we increased fillet radii from R5 to R10 at critical junctions and placed chromite sand to accelerate cooling and mitigate stress concentration.
The optimized steel casting process was validated through another set of trial productions. Two castings were sectioned for internal inspection, revealing dense, defect-free structures with no shrinkage porosity. The other two were machined and measured, demonstrating controlled deformation and compliance with dimensional tolerances. The final steel castings exhibited excellent surface quality after machining, meeting all design specifications for the equipment. Subsequent batch production confirmed the reliability of the process, enabling the integration of these steel castings into full assemblies without issues.
In conclusion, this study successfully developed and refined a steel casting process for large frame guide rails, overcoming typical defects through a combination of traditional design principles and modern simulation. The use of ProCAST allowed us to visualize and address solidification and stress-related problems, leading to practical modifications that enhanced the quality of steel castings. Key lessons include the importance of integrated riser systems, tailored shrinkage allowances, and strategic gating for complex geometries. This work not only solves a specific production challenge but also provides a framework for similar large frame steel castings, promoting the adoption of casting over welding for high-performance components. The steel casting industry can benefit from such holistic approaches, where simulation-driven optimization complements empirical knowledge to achieve superior results.
Further considerations for steel casting process design involve continuous monitoring of parameters such as cooling rates and alloy composition. The modulus method remains a valuable tool, but it can be enhanced with computational fluid dynamics (CFD) simulations to predict flow patterns. For feeding efficiency, the required riser volume can be estimated using Chvorinov’s rule, where solidification time \(t_s\) is proportional to the square of the modulus: $$t_s = k \cdot M^2$$ where \(k\) is a constant dependent on mold material. In our steel casting process, we ensured that risers had larger moduli than the casting sections they feed, typically by a factor of 1.1 to 1.2. Additionally, the thermal gradient \(G\) and solidification rate \(R\) influence microstructure; optimizing these through controlled cooling can improve mechanical properties in steel castings. The relationship is often expressed as: $$G \cdot R = \text{constant}$$ for a given alloy. By managing these factors, we can produce steel castings with consistent performance across large frames.
In summary, the journey from initial design to final production of this steel casting guide rail underscores the iterative nature of foundry engineering. Each defect analysis spurred improvements, leveraging both simulation and practical adjustments. The success of this project highlights the potential for steel casting to manufacture critical large-scale components with precision and reliability, paving the way for broader applications in heavy machinery and equipment manufacturing.
