During durability testing of a 2.0T engine with aluminum alloy main bearing covers manufactured through high-pressure die casting (HPDC), catastrophic fractures occurred at multiple bearing cap locations after 567 hours of operation. This study investigates the root causes through multi-disciplinary analysis and proposes effective structural and process improvements.

1. Fracture Mechanism Analysis
The fracture originated near ejector pin marks on the non-crankshaft side, showing typical brittle fracture characteristics. Metallurgical analysis revealed critical casting defects influencing material properties:
Location | Microstructure Characteristics | Tensile Strength (MPa) |
---|---|---|
Section 1-2 | Lamellar eutectic silicon, primary silicon particles | 125 (Failed) |
Section 3-4 | Spheroidized eutectic silicon | 185 (Pass) |
The material strength degradation follows the relationship:
$$ \sigma_b = \sigma_0(1 – f_d)^{n} $$
Where:
$\sigma_b$ = actual tensile strength
$\sigma_0$ = ideal material strength (180 MPa)
$f_d$ = defect area ratio (0.32 measured)
$n$ = stress concentration factor (1.8 for lamellar structures)
2. Process-Induced Stress Concentrations
X-ray analysis confirmed severe gas porosity and shrinkage cavities in critical load-bearing regions, reducing effective cross-sectional area by 18-22%. The combined effect of casting defects and improper ejector pin placement created stress intensification:
$$ K_t = 1 + 2\sqrt{\frac{a}{\rho}} $$
Where:
$K_t$ = stress concentration factor
$a$ = defect depth (1.2 mm)
$\rho$ = fillet radius (0.5 mm)
3. Fatigue Life Simulation
Finite element analysis revealed critical safety factors below design requirements:
Bearing Position | Original Design SF | Optimized Design SF |
---|---|---|
MB1 | 1.38 | 2.06 |
MB2 | 0.95 | 1.34 |
MB3 | 1.44 | 2.17 |
The modified fatigue life equation accounts for casting defects:
$$ N_f = \frac{C}{(\Delta \sigma \cdot K_t)^m} $$
Where:
$N_f$ = cycles to failure
$\Delta \sigma$ = stress amplitude
$C,m$ = material constants
4. Design and Process Optimization
Key improvements addressed both structural and casting defect issues:
- Top rib elimination reducing wall thickness from 12mm → 8mm
- Ejector pin relocation to non-critical areas
- Enhanced cooling with local squeeze pin technology
- Process parameter optimization:
- Injection pressure: 80 MPa → 95 MPa
- Mold temperature: 180°C → 220°C
5. Validation Results
Post-optimization verification showed significant improvements:
Parameter | Original | Optimized |
---|---|---|
Tensile Strength | 125 MPa | 162 MPa |
Defect Area Ratio | 32% | 8% |
Durability Hours | 567 | 800+ |
The optimized design successfully passed 3,000 thermal cycles and 800-hour endurance testing without failure, demonstrating effective resolution of casting defect-induced fractures.
6. Conclusion
This study establishes a comprehensive approach for addressing HPDC component failures through synergistic design and process improvements. Critical factors include:
- Strategic avoidance of stress concentrators near casting defect zones
- Microstructure control through thermal management
- Systematic fatigue life prediction incorporating defect parameters
The methodology provides valuable guidance for developing reliable aluminum cast components in high-load engine applications.