Analysis and Optimization of Main Bearing Cover Fracture in High-Pressure Die Casting Engine Components

During durability testing of a 2.0T engine with aluminum alloy main bearing covers manufactured through high-pressure die casting (HPDC), catastrophic fractures occurred at multiple bearing cap locations after 567 hours of operation. This study investigates the root causes through multi-disciplinary analysis and proposes effective structural and process improvements.

1. Fracture Mechanism Analysis

The fracture originated near ejector pin marks on the non-crankshaft side, showing typical brittle fracture characteristics. Metallurgical analysis revealed critical casting defects influencing material properties:

Location Microstructure Characteristics Tensile Strength (MPa)
Section 1-2 Lamellar eutectic silicon, primary silicon particles 125 (Failed)
Section 3-4 Spheroidized eutectic silicon 185 (Pass)

The material strength degradation follows the relationship:

$$ \sigma_b = \sigma_0(1 – f_d)^{n} $$

Where:
$\sigma_b$ = actual tensile strength
$\sigma_0$ = ideal material strength (180 MPa)
$f_d$ = defect area ratio (0.32 measured)
$n$ = stress concentration factor (1.8 for lamellar structures)

2. Process-Induced Stress Concentrations

X-ray analysis confirmed severe gas porosity and shrinkage cavities in critical load-bearing regions, reducing effective cross-sectional area by 18-22%. The combined effect of casting defects and improper ejector pin placement created stress intensification:

$$ K_t = 1 + 2\sqrt{\frac{a}{\rho}} $$

Where:
$K_t$ = stress concentration factor
$a$ = defect depth (1.2 mm)
$\rho$ = fillet radius (0.5 mm)

3. Fatigue Life Simulation

Finite element analysis revealed critical safety factors below design requirements:

Bearing Position Original Design SF Optimized Design SF
MB1 1.38 2.06
MB2 0.95 1.34
MB3 1.44 2.17

The modified fatigue life equation accounts for casting defects:

$$ N_f = \frac{C}{(\Delta \sigma \cdot K_t)^m} $$

Where:
$N_f$ = cycles to failure
$\Delta \sigma$ = stress amplitude
$C,m$ = material constants

4. Design and Process Optimization

Key improvements addressed both structural and casting defect issues:

  1. Top rib elimination reducing wall thickness from 12mm → 8mm
  2. Ejector pin relocation to non-critical areas
  3. Enhanced cooling with local squeeze pin technology
  4. Process parameter optimization:
    • Injection pressure: 80 MPa → 95 MPa
    • Mold temperature: 180°C → 220°C

5. Validation Results

Post-optimization verification showed significant improvements:

Parameter Original Optimized
Tensile Strength 125 MPa 162 MPa
Defect Area Ratio 32% 8%
Durability Hours 567 800+

The optimized design successfully passed 3,000 thermal cycles and 800-hour endurance testing without failure, demonstrating effective resolution of casting defect-induced fractures.

6. Conclusion

This study establishes a comprehensive approach for addressing HPDC component failures through synergistic design and process improvements. Critical factors include:

  • Strategic avoidance of stress concentrators near casting defect zones
  • Microstructure control through thermal management
  • Systematic fatigue life prediction incorporating defect parameters

The methodology provides valuable guidance for developing reliable aluminum cast components in high-load engine applications.

Scroll to Top