In the production of engine cylinder heads, particularly for models like the WP10, various metal casting defects frequently arise, leading to high rejection rates. These metal casting defects, such as porosity, sand inclusions, and sintering, significantly impact product quality and manufacturing efficiency. Based on my experience in foundry processes, I will detail the analysis and improvements implemented to address these issues. The WP10 cylinder head has a sand mold dimensions of 1200 mm × 900 mm × 300/300 mm, producing eight pieces per mold with a total pouring weight of 220 kg and an initial pouring temperature of 1400–1420°C. The casting wall thickness generally ranges from 5 mm to 30 mm at bolt holes, where sintering defects commonly occur near the gates. The molding process uses green sand for the upper and lower molds, while core components like the upper and lower sandwich cores, intake and exhaust passage cores, tappet cores, and injector nozzle cores are made from coated sand. The large skin core employs cold box technology, assembled before coating, but the complexity often leads to gas-related metal casting defects. In small-batch production, the primary metal casting defects included porosity, sand holes, and localized sintering, with a comprehensive rejection rate exceeding 6.2% and machining-induced gas porosity at around 2%. This article focuses on analyzing these metal casting defects and proposing process improvements from a casting perspective.
The formation of metal casting defects, especially porosity, is a critical concern in foundry operations. For the WP10 cylinder head, the intricate core design and high gas evolution from coated sand contribute significantly to these issues. Initially, the pouring time per mold was 24–26 seconds, and post-pouring observations showed that many vent pins remained unfilled, indicating inadequate gas escape. After machining, concentrated porosity defects were evident in the middle bridge area of the cylinder head. To address this, I analyzed the gating system and排气 mechanisms, implementing changes that reduced pouring time and enhanced venting. The improvements not only mitigated porosity but also laid the foundation for tackling other metal casting defects like sand inclusions and sintering.
Analysis and Improvement of Porosity Defects
Porosity is one of the most prevalent metal casting defects in cylinder head production, primarily due to the high gas generation from complex cores. In the WP10 cylinder head, the use of coated sand cores results in substantial gas evolution during pouring, leading to侵入性气孔 (intrusive porosity). The condition for pore formation can be described by the inequality: $$P_{\text{gas}} \geq \Sigma P$$ where $$\Sigma P = P_{\text{static}} + P_{\text{resistance}} + P_{\text{cavity}}$$ Here, \(P_{\text{gas}}\) represents the gas pressure generated from core decomposition, and \(\Sigma P\) is the total opposing pressure from the molten metal, including static pressure, flow resistance, and cavity pressure. When this inequality holds, gas infiltrates the metal, forming pores. For thin-walled gray iron cylinder heads, an optimal pouring rate of 8–10 kg/s is recommended to minimize such metal casting defects.
Initially, the gating system had a cross-sectional area ratio of \(F_{\text{直}}: F_{\text{横}}: F_{\text{内}} = 1:1.18:1.63\), resulting in a pouring time of 24–26 seconds per mold. This excessive openness caused incomplete filling of vent pins. To reduce the openness ratio, I modified the gating system by increasing the cross-sectional areas of the sprue and runner. The revised ratio became \(F_{\text{直}}: F_{\text{横}}: F_{\text{内}} = 1.04:1:1.3\), which shortened the pouring time to 19–22 seconds per mold. This adjustment improved metal flow and reduced gas entrapment, effectively addressing one of the key metal casting defects. The table below summarizes the gating system changes:
| Component | Original Ratio | Improved Ratio | Pouring Time (s) |
|---|---|---|---|
| Sprue (F_直) | 1 | 1.04 | 24–26 to 19–22 |
| Runner (F_横) | 1.18 | 1 | |
| Ingate (F_内) | 1.63 | 1.3 |
Additionally, I focused on排气 improvements to combat localized porosity in slow-cooling areas like the middle bridge. By adding a vent pin with a diameter of 10 mm and height of 100 mm in this region, I enhanced gas escape and accelerated cooling, acting as a chill to balance temperature gradients. The vent pin installation increased \(P_{\text{resistance}}\), helping to prevent gas intrusion. Furthermore, I revised the sealing method for vent cores by replacing compressed asbestos gaskets with a planar sealing technique where the upper sand mold presses down, reducing leaks and subsequent metal casting defects. These steps collectively reduced porosity-related rejections, demonstrating how targeted adjustments can mitigate common metal casting defects.
Analysis and Improvement of Sand Inclusion Defects
Sand inclusions are another category of metal casting defects that plagued the WP10 cylinder head production, manifesting as fixed sand holes beneath vent pins or random scattered sand on various surfaces. The root cause was identified as residual sand at vent pin junctions due to excessive drilling depth and inadequate cleaning. In the original setup, vent pins on the upper mold plate had a height of 250 mm, and drilling operations often left sand deposits at the interfaces, which were difficult to remove during blowing. This led to consistent sand holes in specific locations, exacerbating metal casting defects.
To resolve this, I increased the vent pin height from 250 mm to 295 mm and reduced the drilling depth by 30 mm. This elevated the sand deposit junction, making it easier for operators to blow away residues during cleaning. The modification significantly reduced sand inclusion defects. Moreover, to address random scattered sand on the upper mold surface, I introduced an automated blowing system that removes loose sand before mold closing. This system, integrated into the production line, ensures thorough cleaning without manual intervention, further minimizing metal casting defects. The following table outlines the key parameters for sand inclusion improvements:
| Aspect | Original Value | Improved Value | Impact |
|---|---|---|---|
| Vent Pin Height | 250 mm | 295 mm | Easier sand removal |
| Drilling Depth Reduction | N/A | 30 mm | Reduced sand retention |
| Cleaning Method | Manual blowing | Automated blowing system | Consistent cleaning |
In addition, I optimized the machining allowances on the cylinder head bottom surface to eliminate subtle sand holes in critical areas like the combustion chamber. By increasing the machining allowance by 0.5 mm in these regions, I ensured that any residual sand inclusions would be removed during processing, thus reducing the incidence of metal casting defects that compromise engine performance. The integration of these measures highlights a comprehensive approach to tackling sand-related metal casting defects through both process and equipment enhancements.

Analysis and Improvement of Sintering Defects
Sintering defects represent a significant challenge in metal casting, particularly in thick-walled sections near gates. For the WP10 cylinder head, sintering occurred primarily around bolt holes adjacent to the ingate, where the wall thickness reaches 30 mm. Prolonged exposure to high-temperature molten metal caused the sand cores to sinter, leading to surface imperfections and increased rejection rates. Analysis revealed that the nominal wall thickness was 35 mm in these areas, with a machined thickness of 6.3 mm per side, which was at the upper limit of the design specification of 5 mm ± 1.0 mm. This excess thickness contributed to the sintering metal casting defects by extending the thermal load on the cores.
To mitigate this, I increased the core thickness in the susceptible areas by 1.0 mm, enhancing its thermal resistance. This adjustment reduced the heat exposure time, thereby decreasing sintering incidents. Additionally, I applied a zirconia-based coating to these cores, leveraging its high refractoriness to withstand elevated temperatures. The zirconia coating improved the core’s durability against thermal degradation, addressing one of the persistent metal casting defects in the production line. The effectiveness of these changes can be expressed using a simple thermal model: $$Q = k \cdot A \cdot \Delta T \cdot t$$ where \(Q\) is the heat transferred, \(k\) is the thermal conductivity, \(A\) is the area, \(\Delta T\) is the temperature difference, and \(t\) is time. By increasing core thickness and using refractory coatings, I reduced \(Q\) and \(t\), minimizing sintering. The table below summarizes the sintering improvements:
| Parameter | Original State | Improved State | Effect on Sintering |
|---|---|---|---|
| Core Thickness | Baseline | +1.0 mm | Increased thermal resistance |
| Coating Type | Standard | Zirconia-based | Higher refractoriness |
| Wall Thickness | 35 mm (max) | Optimized to spec | Reduced heat retention |
These interventions not only reduced sintering defects but also improved overall casting integrity, demonstrating how material and dimensional adjustments can combat specific metal casting defects. The continuous monitoring and refinement of these parameters are essential for sustaining low rejection rates in high-volume production.
Results and Conclusion
After implementing the described improvements, the comprehensive rejection rate for WP10 cylinder heads decreased significantly. Over a three-month period, the rate consistently remained below 1.5%, down from over 6.2%, indicating the effectiveness of the measures against various metal casting defects. The table below illustrates the monthly rejection trend, highlighting the progress achieved through process optimization:
| Month | Rejection Rate (%) | Key Improvements Implemented |
|---|---|---|
| Initial Baseline | 6.20 | N/A |
| Month 1 | 3.43 | Gating system modification |
| Month 2 | 3.23 | Vent pin adjustments |
| Month 3 | 2.91 | Automated blowing system |
| Month 4 | 2.26 | Core thickness increase |
| Month 5 | 1.10 | Zirconia coating application |
| Stabilization Period | <1.5 | All improvements integrated |
In conclusion, addressing metal casting defects requires a holistic approach that combines theoretical analysis with practical modifications. Key takeaways include: optimizing gating system ratios to control pouring speed, which effectively reduces porosity; adding vent pins in slow-cooling zones to dissipate gases; enhancing sealing methods to prevent gas leaks; adjusting process parameters to eliminate sand inclusions; and refining core designs with refractory materials to combat sintering. Each of these strategies contributes to a robust casting process, minimizing metal casting defects and improving product quality. Future work should focus on continuous monitoring and advanced simulations to further reduce variability in casting outcomes, ensuring that metal casting defects are kept at bay in high-performance applications.
