Casting Defect Analysis and Process Optimization in High-Performance Diesel Engine Cylinder Block Production

1. Technical Requirements and Production Conditions

The RuT450 cylinder block for 8Y-series diesel engines presents significant casting challenges due to its complex geometry (880 mm × 560 mm × 430 mm) and varying wall thickness (4.5-61 mm). Key material specifications include:

Element Composition (%)
C 3.65-3.85
Si 1.80-2.20
Mn 0.30-0.50
Cu 0.80-0.90
Sn 0.08-0.09

The casting process employs OCC wire feeding treatment and HWS squeeze molding, with pouring parameters governed by:

$$ T_p = 1430 \pm 10^{\circ}\text{C} $$
$$ t_f = 22 \pm 3\ \text{s} $$

2. Critical Casting Defects and Root Cause Analysis

2.1 Mold Leakage Defects

Leakage defects occurring at gear chamber flanges (defect rate 41.67%) were traced to core positioning errors and inadequate sealing at sand core interfaces. The leakage potential (L_p) can be expressed as:

$$ L_p = \frac{\Delta x}{d_m} \times 100\% $$

Where Δx represents core misalignment and d_m denotes mating surface clearance.

2.2 Shrinkage Porosity Formation

Concentrated shrinkage cavities in inter-cylinder thick sections (defect rate 37.50%) resulted from inappropriate solidification control. The shrinkage susceptibility index (S_s) for compacted graphite iron follows:

$$ S_s = \frac{(CE – 4.3)^2}{0.1} + \frac{(T_p – 1400)}{10} $$

Where CE represents carbon equivalent calculated as:

$$ CE = \mathrm{C} + \frac{\mathrm{Si} + \mathrm{P}}{3} $$

Parameter Initial Value Critical Range
CE 4.25-4.58 >4.35
Pouring Temp 1430°C <1410°C

3. Process Optimization Strategies

3.1 Mold Leakage Countermeasures

Implementation of dual corrective actions:

Measure Implementation Effect
Core Alignment 0.1mm positioning accuracy Defect rate ↓58%
Interface Sealing Ceramic gasket installation Leakage paths ↓96%

3.2 Shrinkage Control Protocol

Modified metallurgical parameters:

$$ CE_{\text{new}} = 4.42 \pm 0.05 $$
$$ T_p^{\text{opt}} = 1410 \pm 5^{\circ}\text{C} $$

Elemental adjustment matrix:

Element Original (%) Optimized (%)
C 3.70 3.82
Si 1.88 2.15
Mn 0.45 0.35

4. Implementation Results

The integrated approach demonstrated remarkable defect reduction:

Defect Type Initial Rate Final Rate Improvement
Mold Leakage 41.67% 0% 100%
Shrinkage 37.50% 0% 100%

The quality enhancement followed the relationship:

$$ Q_{\text{index}} = \frac{\sum(Defect_{\text{initial}} – Defect_{\text{final}})}{\sum Defect_{\text{initial}}} \times 100\% = 100\% $$

5. Metallurgical Process Control

Critical control parameters for stable production:

$$ \text{Cooling Rate} = \frac{T_p – T_s}{t_s} $$

Where T_s represents solidus temperature (1150°C) and t_s denotes solidification time.

Process Stage Control Parameter Optimal Value
Melting CE Value 4.40±0.05
Pouring Superheat 150-160°C
Solidification Cooling Rate 25-30°C/min

6. Conclusion

This systematic approach to casting defect control successfully addressed both mold leakage and shrinkage porosity challenges in compacted graphite iron cylinder block production. The implemented solutions demonstrate that precise process parameterization combined with mechanical improvements can effectively eliminate complex casting defects in high-performance engine components.

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