This study focuses on improving the manufacturing process of B10-type motor housings through comprehensive analysis of casting defects in steel castings. By implementing optimized sand molding techniques and modified process parameters, we achieved significant quality improvements while maintaining cost efficiency.

1. Process Parameter Optimization
For steel casting production, the chemical composition control proves critical for defect prevention. The optimized element ranges are:
| Element | Range (%) | Impact on Hot Tearing |
|---|---|---|
| C | 0.20-0.25 | Maximizes crack resistance |
| Si | 0.25-0.45 | Enhances fluidity |
| Mn | 0.60-0.68 | Neutralizes sulfur |
| S | ≤0.015 | Reduces low-melting phases |
The crack formation mechanism can be expressed through thermal strain analysis:
$$ \varepsilon \geq \delta $$
Where $\varepsilon$ represents actual strain and $\delta$ denotes critical fracture strain at the brittle temperature range.
2. Sand System Selection
Comparative analysis of molding processes reveals distinct performance characteristics:
| Parameter | Furan Resin | Alkaline Phenolic |
|---|---|---|
| Hot Strength (MPa) | 3.2-4.5 | 2.8-3.6 |
| Sulfur Migration (ppm) | 120-180 | 15-25 |
| Collapsibility Index | 0.45 | 0.68 |
The alkaline phenolic resin system demonstrates superior performance for steel casting applications, particularly in reducing hot tearing tendency through improved sand system yielding:
$$ Y = \frac{\sigma_{sand}}{\sigma_{metal}} \times 100\% $$
Where $Y$ represents the yield compliance ratio between sand mold and casting metal.
3. Gating System Redesign
Modified bottom-gating design reduced turbulence index by 42%:
$$ T_f = \frac{Q}{A\sqrt{2gh}} $$
Where:
$T_f$ = Turbulence factor
$Q$ = Flow rate (kg/s)
$A$ = Choke area (m²)
$g$ = Gravitational acceleration
$h$ = Metallostatic head
4. Production Verification
Process optimization yielded measurable quality improvements in steel casting production:
| Metric | Pre-Optimization | Post-Optimization |
|---|---|---|
| Cracks/Unit | 60 | 8 |
| Sand Inclusion Defects | 80 | 18 |
| Scrap Rate (%) | 19 | 1.1 |
| Welding Cost (USD/unit) | 486 | 260 |
The modified steel casting process demonstrates 78% reduction in quality-related costs while maintaining dimensional accuracy within ASTM A802 Class II requirements.
5. Economic Analysis
Cost comparison of molding materials per ton steel casting:
| Component | Furan System | Phenolic System |
|---|---|---|
| Resin Cost | $787 | $812 |
| Sand Cost | $700 | $940 |
| Total | $1,487 | $1,752 |
Despite 17.8% higher material costs, the alkaline phenolic system achieves 61.3% lower total production costs through reduced rework and improved yield in steel casting operations.
6. Technical Limitations
Current challenges in steel casting optimization include:
$$ R_r = \frac{W_r}{W_t} \times 100\% $$
Where $R_r$ represents reclaimed sand ratio (68-72% for phenolic systems vs 85-90% for furan), indicating need for improved sand reclamation techniques.
This comprehensive approach to steel casting process optimization demonstrates effective defect control through systematic parameter adjustment and material science application, providing valuable insights for complex casting manufacturing.
