Influence of Pouring Position on Steel Casting Process for Shell-Type Components

This paper analyzes critical factors affecting the quality and efficiency of steel casting processes for large shell-type components through empirical case studies. By optimizing pouring positions and solidification control strategies, we demonstrate significant improvements in yield rates and defect reduction.

1. Technical Requirements and Process Challenges

The shell component (Fig. 1) features complex geometry with thickness variations from 18mm to 130mm. Key challenges include:

Parameter Specification
Chemical Composition C:0.19-0.29%, Si:0.25-0.65%, Mn:0.40-0.80%
Mechanical Properties Rm≥450MPa, Z≥18%, HB:130-170
Quality Standards ASTM E446 Level II/III, GB7233-2009 Level I

The solidification modulus (M) varies significantly across sections:

$$M = \frac{V}{A}$$

Where V = volume (m³) and A = cooling surface area (m²). Critical sections show modulus ratios up to 7.2:1.

2. Initial Process Limitations

The original steel casting process with C-groove upward orientation exhibited several drawbacks:

Parameter Initial Process
Yield Rate 41.0%
Pouring Weight 5100kg
Defect Rate 23% (sand inclusion/gas porosity)

The Reynolds number during pouring reached critical turbulence levels:

$$Re = \frac{\rho v d}{\mu} > 4000$$

Where ρ = density (kg/m³), v = velocity (m/s), d = characteristic length (m), μ = viscosity (Pa·s).

3. Optimized Steel Casting Process

The modified process features C-groove downward orientation with bottom-gating system:

Improvement Technical Solution
Solidification Control Exothermic risers (η=32%) vs. sand risers (η=14%)
Gating Design 4-bottom gates with Fsprue:Frunner:Fgate = 1:2:3.38
Process Yield 61.5% (3400kg pouring weight)

The Niyama criterion confirms improved feeding:

$$N = \frac{G}{\sqrt{\dot{T}}} > 1\,^{\circ}C^{1/2}/min^{1/2}$$

Where G = temperature gradient (°C/m), Ṫ = cooling rate (°C/s).

4. Defect Reduction Mechanism

The optimized steel casting process reduces turbulence energy by 68%:

$$E_t = \frac{1}{2}\rho v^2 < 150\,J/kg$$

Key improvements include:

  • Entrained slag inclusion probability reduced from 0.42 to 0.07
  • Gas porosity index decreased by 83%
  • Dimensional accuracy improved to IT13-IT15

5. Production Efficiency Gains

The steel casting process optimization enables:

Metric Improvement
Pouring Capacity 2 castings/ladle (7500kg)
Solidification Time 65s (34% reduction)
Energy Consumption 9.8kWh/ton (-27%)

The thermal efficiency of exothermic risers follows:

$$Q_{exo} = m[\Delta H + c_p(T_m – T_a)]$$

Where m = riser mass (kg), ΔH = reaction heat (kJ/kg), cp = specific heat (kJ/kg°C).

6. Conclusion

This steel casting process optimization demonstrates that proper pouring position selection combined with scientific feeding system design can achieve:

  • Yield rate improvement: 41.0% → 61.5%
  • Defect rate reduction: 23% → 4.7%
  • Production capacity doubling: 1 → 2 castings/ladle

The methodology provides valuable insights for similar steel casting applications requiring complex geometry and high quality standards.

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