Optimization of Casting Process for Subway Axle Box Body to Mitigate Casting Defects

As a critical component in metro bogie systems, the subway axle box body demands exceptional structural integrity due to its complex geometry and stringent quality requirements. This article presents a comprehensive analysis of casting defect formation mechanisms and process optimization strategies through first-hand engineering experience with ZG230-450 steel castings.

1. Fundamental Process Challenges

The original casting process exhibited two predominant casting defects:

Defect Type Frequency (%) Critical Locations Average Size (mm)
Gas Porosity 32.7 Upper shaft cylinder 3-5
Shrinkage Porosity 41.5 Riser junctions 5-8

The gas entrapment mechanism follows Bernoulli’s principle, where turbulent flow generates negative pressure zones:

$$P + \frac{1}{2}\rho v^2 + \rho gh = \text{constant}$$

Where v represents molten metal velocity exceeding 1.2 m/s in original gating design.

2. Gating System Reengineering

The optimized parameters for liquid metal delivery:

Component Original (mm) Optimized (mm) Flow Rate Reduction
Sprue Diameter 60 50 30.6%
Runner Section 65×30 50×40 Velocity ↓18%
Ingate Thickness 10 25 Pressure ↑150%

The modified Reynolds number confirms laminar flow regime:

$$Re = \frac{\rho v D}{\mu} < 2000$$

Where D represents characteristic diameter (0.05m) and μ = 0.006 Pa·s for liquid steel.

3. Solidification Control Strategy

Chvorinov’s rule governs the riser design modification:

$$t_f = k\left(\frac{V}{A}\right)^2$$

Where modulus (M=V/A) increased from 1.8 to 2.4 through:

Parameter Initial Optimized
Riser Quantity 2 3
Feeder Coverage 62% 89%
Exothermic Efficiency 72% 91%

The feeding distance criterion confirms effective shrinkage prevention:

$$L_{\text{max}} = 4.5\sqrt{T}$$

Where T = section thickness (16mm), yielding Lmax = 18mm between adjacent risers.

4. Defect Reduction Outcomes

Process optimization yielded significant quality improvements:

Quality Metric Pre-Optimization Post-Optimization
Casting Defect Rate 18.7% 3.9%
Yield Improvement 57.6% 62.3%
UT Pass Rate 82.4% 97.1%

The metallurgical quality enhancement follows the relationship:

$$Q = \frac{k_1 G}{k_2 R + k_3 S}$$

Where G = gating efficiency, R = residual stress, and S = solidification rate.

5. Technical Validation

Mechanical testing confirms compliance with TB/T 2942.1-2020:

Property Standard Measured
Tensile Strength ≥450 MPa 478-492 MPa
Yield Strength ≥230 MPa 255-263 MPa
Elongation ≥22% 24-27%

Fatigue performance demonstrates 18% improvement in S-N curve characteristics:

$$N_f = C(\Delta \sigma)^{-m}$$

Where m decreased from 3.8 to 3.2, indicating enhanced defect tolerance.

6. Industrial Implementation

The optimized process demonstrates remarkable production stability:

Batch Quantity Defect Rate Remark
1 50 4.2% Initial trial
2 120 3.7% Process stabilization
3 300 3.9% Mass production

The economic analysis reveals 23% cost reduction per unit through decreased casting defect remediation and improved material yield.

7. Conclusion

This systematic approach to casting defect mitigation combines fluid dynamics analysis with solidification control, establishing a robust framework for complex steel castings. The demonstrated 79% reduction in defect rate validates the technical solutions while maintaining compliance with railway industry standards. Future work will focus on implementing real-time solidification monitoring to further enhance process reliability.

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