Optimization of Steel Casting Process for Axle Box Body in Railway Applications

With increasing demands on railway vehicle speed and load capacity, the quality requirements for steel castings in bogie systems have intensified. This paper presents a systematic improvement strategy addressing defects observed during the production of axle box bodies – critical load-bearing components in metro vehicle bogies. Through structural analysis and process optimization, we achieved significant quality enhancements in these thin-walled box-type steel castings.

1. Structural Characteristics and Process Challenges

The axle box body, made from ZG25MnCrNiMo (Grade C steel), features complex geometry with wall thickness ranging 20-30 mm. Key process parameters include:

Parameter Value
Weight 95 kg
Shrinkage allowance 2%
Pouring temperature 1,560-1,580°C
Molding material CO₂-hardened sodium silicate sand

The original casting process exhibited multiple defects including shrinkage porosity (12% occurrence), sand inclusion (8%), and dimensional inaccuracies (5% rejection rate). Through defect analysis, we identified three critical improvement areas:

$$ f(x) = k \cdot \frac{V}{A} \cdot \sqrt{\frac{T_m – T_p}{\rho \cdot c}} $$

Where k represents the mold material constant, V/A the volume-surface area ratio, and Tm, Tp the melting and pouring temperatures respectively.

2. Defect Analysis and Solutions

2.1 Sand Erosion in Thin Sections

The 50mm-deep rib cavity between large/small axle sleeves showed consistent sand erosion. Our solution combined:

  • Reinforced core design with embedded steel pins
  • Modified core binder composition (Table 1)
Table 1: Core Strength Comparison
Parameter Original Improved
Compressive strength (MPa) 1.2 2.5
Erosion resistance index 65 92
Shakeout performance Grade C Grade B

2.2 Shrinkage Porosity in Thick Sections

The original riser design failed to maintain directional solidification in the 245mm-high axle sleeve. Modified riser configuration achieved better feeding efficiency:

$$ L_f = \frac{4.5 \cdot t}{\sqrt{M}} $$

Where Lf is feeding distance, t section thickness, and M the casting modulus. Key improvements included:

  • Increased riser quantity from 2 to 3
  • Changed riser shape from elliptical to circular
  • Reduced inter-riser distance by 25%

3. Process Optimization Details

3.1 Gating System Redesign

Relocating the ingate from central ribs to machined surfaces eliminated crack formation. The new gating ratio (1:1.5:2) ensures laminar flow while maintaining adequate feeding pressure:

$$ v = \frac{Q}{A} = \frac{0.85 \cdot g \cdot H^{0.5}}{\mu} $$

Where v is metal velocity, Q flow rate, and H metallostatic head.

3.2 Core Positioning System

The redesigned spring seat core achieved ±0.5mm positioning accuracy through:

  • Dual lateral locators instead of single bottom support
  • Reduced core seat clearance from 3mm to 1mm
  • Triangular reinforcement ribs in core structure

4. Production Verification

Implementing these improvements in 10 trial castings yielded:

Quality Indicator Original Improved
Surface defects per m² 3.2 0.4
UT rejection rate 15% 0%
Machining allowance consistency ±2.5mm ±0.8mm

The optimized steel casting process demonstrates how systematic analysis and targeted improvements can significantly enhance the quality of complex railway components. This methodology provides a template for addressing similar challenges in heavy-section steel castings across industries.

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