Optimizing Casting Process for Excavator Boom Connection Part Using Numerical Simulation

During excavator operation, the boom-to-frame connection component endures multidirectional alternating loads. Traditional welded fabrication carried fracture risks at joints. Switching to casting significantly reduced both production costs and failure probabilities. This study details how ProCAST simulation optimized the process for a critical excavator casting part, eliminating defects while ensuring quality.

The ZG25 steel excavator casting part measured 754 mm × 171 mm, featuring thin walls (minimum 15 mm) and thick sections (maximum 67 mm). Key requirements included:

  • Zero shrinkage porosity or inclusions
  • Surface cracks ≤ 2 mm via fluorescent magnetic particle inspection

Initial horizontal casting setup used CO₂-hardened sodium silicate sand molds. Two Φ150 mm × 300 mm risers were placed at thick-section bosses (Figure 2). Chiller configurations were evaluated to manage thermal stress:

Scheme Chiller Position Dimensions (mm)
1 Part bottom 32 × 40 × 750
2 Thick sections 32 × 30 × 120 × 2
3 None

ProCAST simulations modeled filling, solidification, and stress using these parameters:

  • Mesh: 10 mm (part), 40 mm (mold)
  • Pouring time: 25 s
  • Pouring temperature: 1565°C
  • Interface heat transfer:
    $$ h_{chiller/part} = 2000 \text{W/(m²·K)} $$
    $$ h_{mold/sand} = 300 \text{W/(m²·K)} $$

Results for the critical excavator casting part revealed:

Parameter Scheme 1 Scheme 2 Scheme 3
Filling time (s) 25.0 25.0 24.1
Avg. solid fraction at fill end (%) 14.9 10.9 11.2
Total solidification time (s) 4918 5020 5041
Peak core temperature (°C) 1421.0 1420.0 1594.7

Hot tearing risk was quantified using the Hot Tearing Indicator (HTI):

$$ HTI = \frac{\sigma_{effective}}{E \cdot \alpha \cdot \Delta T} $$

where $\sigma_{effective}$ is von Mises stress, $E$ is Young’s modulus, $\alpha$ is thermal expansion coefficient, and $\Delta T$ is temperature drop. Critical zone values:

Scheme HTI Max. stress (kPa)
1 0.0042 316 (y-direction)
2 0.0029 150 (y-direction)
3 0.0030 222 (y-direction)

Scheme 1’s high HTI correlated with actual thermal cracks (Figure 4). Though Scheme 2 reduced HTI, chillers increased gas defect risks. Scheme 3 avoided chillers but showed core sand burn-in due to excessive temperatures. Final optimization replaced silica sand cores with limestone equivalents, yielding:

$$ HTI_{optimized} = 0.0027 \quad ; \quad \sigma_{y} = 185 \text{kPa} $$

Validated castings exhibited no cracks, minimal inclusions, and eliminated bore burn-in. This excavator casting part process demonstrates how simulation-driven design enhances reliability while reducing trial cycles.

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