In the production of high-strength, thin-walled cylinder blocks for heavy-duty engines, the occurrence of casting holes—specifically blowholes and sand inclusions—poses a significant challenge to yield and quality. As a casting engineer involved in this project, I have extensively analyzed and implemented measures to mitigate these defects. This article delves into the structural and procedural aspects of the B8 1D cylinder block casting process, detailing the root causes of casting holes and the comprehensive solutions applied. The focus is on minimizing gas-related porosity and sand erosion through material, design, and process optimizations. Throughout this discussion, the term “casting holes” will be frequently referenced to emphasize the pervasive nature of these defects in foundry operations.
The B8 1D cylinder block, used in J6 series vehicles, is a complex casting with dimensions of 980 mm × 426 mm × 526 mm and a weight of 283 kg. Its design features thin walls, such as the 5–6 mm thick water jacket cover, and requires multiple sand cores (13 in total) arranged in overlapping layers. This complexity inherently increases the risk of casting holes due to factors like gas evolution from binders, inadequate venting, and sand instability. The original process employed a horizontal parting line with a combination of middle and bottom gating systems, using cold-box cores and high-pressure molding. Despite venting pins and overflow risers, defect rates remained high, with casting holes accounting for over 36% of total scrap, as shown in initial data.

To understand the formation of casting holes, it is essential to analyze the mechanisms behind blowholes and sand inclusions. Blowholes, a type of casting hole, result from trapped gases during metal pouring and solidification. These gases can originate from sand cores, mold materials, or reactions within the molten iron. The gas pressure \( P_g \) must exceed the metallostatic pressure \( P_m \) to form a blowhole, which can be expressed as:
$$ P_g = \frac{nRT}{V} $$
where \( n \) is the moles of gas evolved, \( R \) is the gas constant, \( T \) is the temperature, and \( V \) is the volume. In the original process, high resin content (1.6%) in cores led to excessive gas generation, increasing \( n \) and thus \( P_g \). Additionally, poor venting design limited gas escape, causing localized accumulation and casting holes. Sand inclusions, another form of casting hole, occur when loose sand particles enter the mold cavity, often due to residual sand in vents or core erosion. The probability of sand inclusion \( P_s \) can be modeled as:
$$ P_s = k \cdot \frac{A_s \cdot v}{d} $$
where \( k \) is a constant, \( A_s \) is the sand area exposed, \( v \) is the metal velocity, and \( d \) is the particle diameter. In this case, inadequate cleaning of vent holes and core box issues elevated \( A_s \), leading to frequent casting holes.
The original casting process was characterized by several parameters that contributed to casting holes. A summary is provided in Table 1, highlighting key factors and their impact on defect formation.
| Process Parameter | Original Value | Impact on Casting Holes |
|---|---|---|
| Resin Addition in Cores | 1.6% | High gas evolution, increasing blowhole risk |
| Core Weight (曲轴箱) | 21–23 kg | More binder and gas, promoting casting holes |
| Venting Pin Diameter | 20 mm (明通气针) | Insufficient exhaust area, gas trapping |
| Gating System Design | Sharp transitions | Turbulence, gas entrapment, and sand erosion |
| Pouring Temperature | 1410–1430°C | Lower temperature increases viscosity, hindering gas escape |
| Sand Compactness | 38–45 | High strength but poor permeability, aiding casting holes |
From this analysis, it is clear that multiple factors synergistically led to casting holes. The primary causes included excessive gas from cores, inadequate venting, and sand management issues. To address these, a multi-faceted approach was implemented, focusing on reducing gas sources, enhancing exhaust, and improving sand integrity.
For blowhole reduction, the first step was to minimize gas evolution. This involved switching to a low-gas FS powder in mold coatings, which reduced the gas generation rate \( G \) by approximately 20%, as per laboratory tests. The resin content in cores #9–#13 was lowered from 1.6% to 1.4%, decreasing the gas volume \( V_g \) according to the equation:
$$ V_g = \alpha \cdot w_r $$
where \( \alpha \) is the gas yield coefficient (typically 120–150 cm³/g for cold-box resins) and \( w_r \) is the resin weight. Reducing \( w_r \) directly cut \( V_g \), thus lowering the propensity for casting holes. Additionally, core weight was reduced by incorporating hollow sections in side cores, dropping the mass from 21 kg to 18.6 kg for #7 and from 23 kg to 20.3 kg for #8. This not only saved material but also decreased the total binder amount, further mitigating casting holes.
Venting system enhancements were crucial to prevent gas accumulation. The original design had 34 venting pins, but their layout and size were insufficient. To improve exhaust capacity, three open venting pins were added on the water jacket cover, increasing the total venting area \( A_v \) from 10,676 mm² to 11,618 mm². The exhaust efficiency \( \eta_v \) can be expressed as:
$$ \eta_v = \frac{A_v \cdot C_d}{\sqrt{T}} $$
where \( C_d \) is the discharge coefficient. By enlarging some venting pins from 20 mm to 24 mm and others from 30 mm to 45 mm, and adding connecting channels between vents, \( A_v \) was boosted by an additional 6,488.8 mm². This redesign facilitated smoother gas escape, reducing the local gas pressure \( P_g \) and preventing casting holes. Moreover, venting holes were drilled in core prints to enhance exhaust paths.
The gating system was modified to promote laminar flow and reduce turbulence, which can entrap gas and cause casting holes. The ingate radius was increased to R50–R60 for smoother transitions, lowering the Reynolds number \( Re \):
$$ Re = \frac{\rho v D}{\mu} $$
where \( \rho \) is density, \( v \) is velocity, \( D \) is diameter, and \( \mu \) is viscosity. A lower \( Re \) reduces turbulence, minimizing gas entrapment and sand erosion. The pouring temperature was raised to 1420–1440°C, and pouring time was shortened from 26–28 s to 24–26 s. This elevated temperature field helped maintain fluidity, allowing gases to rise and escape before solidification, thereby addressing casting holes. Table 2 summarizes these blowhole-specific measures.
| Improvement Measure | Technical Detail | Effect on Casting Holes |
|---|---|---|
| Low-gas FS Powder | Reduced gas evolution rate by 20% | Decreased gas volume, fewer blowholes |
| Resin Reduction | From 1.6% to 1.4% in cores | Lower \( V_g \), minimizing casting holes |
| Core Lightening | Hollow sections, weight cut by ~12% | Less binder, reduced gas sources |
| Venting Expansion | Added pins, enlarged diameters, added channels | Increased \( A_v \), better gas exhaust |
| Gating Optimization | Smoother radii, R50–R60 transitions | Reduced turbulence, less gas entrapment |
| Pouring Parameters | Temperature 1420–1440°C, time 24–26 s | Improved fluidity, faster gas escape |
For sand inclusion defects, which are another manifestation of casting holes, the focus was on sand control and process stability. Residual sand in vent holes was a major contributor; thus, operators were trained to clear holes with rods and use air blowers for thorough cleaning. This reduced the sand area \( A_s \) exposed to metal flow, directly lowering \( P_s \) as per the earlier equation. Core box adjustments included removing some ejector pins and venting plugs to prevent sand leakage during core shooting. Additionally, the carbon equivalent (CE) was slightly increased within specification limits to improve metal fluidity and reduce shrinkage, which indirectly minimized sand erosion by stabilizing the flow.
A critical change was adding an ingate at the seventh bearing location. This ensured adequate metal pressure and feeding to the rear section, reducing turbulence that could dislodge sand and create casting holes. The pressure head \( H \) at this point is given by:
$$ H = H_0 – \frac{v^2}{2g} $$
where \( H_0 \) is the initial head, \( v \) is velocity, and \( g \) is gravity. By introducing an ingate, \( H \) was maintained, preventing low-pressure zones that might draw in sand. Wall thickness in critical areas was also increased where possible, enhancing rigidity against sand wash. Cleaning standards were formalized to avoid mechanical damage that could expose casting holes. These sand-related measures are outlined in Table 3.
| Improvement Measure | Technical Detail | Effect on Casting Holes |
|---|---|---|
| Vent Hole Cleaning | Rod clearing and air blowing | Reduced residual sand, lower \( A_s \) |
| Core Box Modification | Removed ejector pins and venting plugs | Less sand leakage, fewer inclusions |
| CE Adjustment | Increased within specs | Better fluidity, reduced shrinkage and erosion |
| Additional Ingate | At seventh bearing | Improved pressure head, less turbulence |
| Wall Thickening | Localized increases | Enhanced resistance to sand wash |
| Cleaning Standardization | Strict protocols for handling | Prevented exposure of latent casting holes |
The combined implementation of these measures led to a significant reduction in casting holes. Within two months, internal scrap rates dropped from 4.19% to 1.005%, and machining scrap rates fell from 3.99% to 2.95%. Blowholes, which had constituted 53.18% of internal scrap, were virtually eliminated in critical areas like the top brackets and bearings. Sand inclusions also decreased markedly, demonstrating the effectiveness of the holistic approach. The success underscores that preventing casting holes requires balancing gas management, venting design, and sand control.
In conclusion, casting holes are a pervasive issue in complex castings like the B8 1D cylinder block, but they can be mitigated through systematic process improvements. Key lessons include the importance of reducing gas sources via material selection and core design, optimizing venting systems to enhance exhaust capacity, and refining gating to ensure smooth metal flow. Regular monitoring and maintenance, such as cleaning vent holes and adjusting CE, are essential for sustained quality. Future work could involve predictive modeling of gas flow using computational fluid dynamics to further minimize casting holes. By sharing these insights, I hope to contribute to broader foundry practices aimed at eliminating casting holes and enhancing casting integrity.
