Research on Oil Leakage Countermeasures in Engine Cylinder Block Main Oil Passage

During durability testing of an engine cylinder block assembly, oil seepage was observed at the main oil passage plug after 8 hours of operation. This study investigates the root cause through thermal expansion analysis and material characterization while proposing an optimized sealing solution.

Thermal Expansion Analysis

The differential thermal expansion between the cast iron engine cylinder block (α = 23×10-6/°C) and steel oil plug (α = 12×10-6/°C) creates critical interfacial gaps. The linear expansion equation:

$$
\Delta L = \alpha \cdot L_0 \cdot \Delta T
$$

Where:
ΔL = Length variation (mm)
α = Thermal expansion coefficient
L₀ = Original length (mm)
ΔT = Temperature change (°C)

For the engine cylinder block main bore (L₀=26mm, ΔT=110°C):

$$
\Delta L_{block} = 23 \times 10^{-6} \times 26 \times 110 = 0.066\ \text{mm}
$$

For the steel plug (ΔT=40°C):

$$
\Delta L_{plug} = 12 \times 10^{-6} \times 26 \times 40 = 0.012\ \text{mm}
$$

Resulting in a thermal gap of:

$$
\text{Gap} = 0.066 – 0.012 = 0.054\ \text{mm}
$$

Material Compatibility Analysis

Parameter Original Sealant Optimized Sealant
Elongation at Break 64% 186%
Shear Strength 1.6 N/mm² 7.0 N/mm²
Breakaway Torque 21 N·m 40 N·m
Thermal Gap Tolerance 0.032mm 0.082mm

Sealant Performance Verification

The modified sealing solution demonstrates superior performance in engine cylinder block applications:

$$
\tau_{\text{max}} = \frac{F_{\text{shear}}}{A_{\text{contact}}}
$$

Where:
τmax = Maximum shear stress
Fshear = Axial load from oil pressure (220N)
Acontact = Effective sealing area (38.5mm²)

For original sealant:

$$
\tau_{\text{original}} = \frac{220}{38.5} = 5.71\ \text{N/mm²} > 1.6\ \text{N/mm²}
$$

For optimized sealant:

$$
\tau_{\text{optimized}} = \frac{220}{38.5} = 5.71\ \text{N/mm²} < 7.0\ \text{N/mm²}
$$

Durability Test Results

Test Parameter Original Sealant Optimized Sealant
Initial Torque 60 N·m 60 N·m
Residual Torque 50.5 N·m 125.9 N·m
Thermal Cycles Failed at 8h Passed 800h
Seepage Occurrence 100% 0%

Conclusion

The engine cylinder block oil leakage mechanism was successfully addressed through:

  1. Thermal expansion compensation through high-elongation sealant
  2. Improved anti-loosening performance (125.9 N·m residual torque)
  3. Enhanced shear resistance (7.0 N/mm² vs 1.6 N/mm²)

The optimized solution demonstrates reliable sealing performance in engine cylinder block main oil passage applications under extreme thermal and mechanical loading conditions.

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