Research on Precision Investment Casting Process for Exhaust Manifolds

With advancements in engine technology, precision investment casting has become critical for manufacturing exhaust manifolds requiring high dimensional accuracy and complex geometries. This study focuses on optimizing the casting process for a heat-resistant austenitic stainless steel (GX40CrNiSi25-20) exhaust manifold using simulation-driven design.

1. Component Characteristics and Material

The exhaust manifold features asymmetric branching channels with significant wall thickness variations (6–20 mm). Key challenges include:

  • Multiple isolated hot spots at junctions
  • Thin-walled sections (minimum 6 mm)
  • High-temperature service requirements (up to 1,100°C)
Element C Cr Ni Mn Si P S Fe
Content (wt%) 0.4 25 20 1 2 0.03 0.03 Bal.

2. Initial Casting Process Design

The gating system employs a stepped configuration with 12 ingates and complementary feeders. Key parameters:

$$ \sum S_{ingate} : \sum S_{runner} : \sum S_{sprue} = 1.4 : 1.2 : 1 $$
$$ v_{pouring} = 2.0\ kg/s,\ T_{pouring} = 1,600^\circ C $$

Parameter Value
Mold Material Zircon Sand
Shell Thickness 6 mm
Heat Transfer Coefficient 500 W/(m²·K)

3. Simulation Analysis

ProCAST simulations revealed critical solidification patterns:

$$ t_{solidification} = \frac{(T_{pour} – T_{eutectic})^2}{\alpha \cdot \Delta T_{critical}} $$

Where $α$ represents thermal diffusivity (3.8×10⁻⁶ m²/s for GX40CrNiSi25-20). Defect-prone areas were identified at channel intersections with localized porosity >1%.

4. Process Optimization

Modified the precision investment casting process through:

  1. Addition of Φ14 mm blind risers at main channel junctions
  2. Implementation of external chills (25 mm thickness) at branch connections
  3. Revised feeder dimensions for improved feeding efficiency
Optimization Before After
Riser Volume 12.8 L 15.2 L
Critical Porosity 1.2–1.8% <0.5%
Yield Rate 58% 63%

5. Solidification Dynamics

The optimized process achieved directional solidification with:

$$ \left( \frac{dT}{dt} \right)_{casting} > \left( \frac{dT}{dt} \right)_{gating} $$

Final solidification occurred in risers rather than functional areas, eliminating internal defects while maintaining dimensional stability within ±0.3 mm.

6. Conclusion

This study demonstrates how precision investment casting combined with numerical simulation can resolve complex manufacturing challenges in exhaust components. The optimized process:

  • Eliminated shrinkage defects completely
  • Improved casting yield by 8.6%
  • Maintained surface roughness Ra ≤ 6.3 μm

The methodology provides a template for developing high-performance castings through systematic process refinement in precision investment casting applications.

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