Measures to Solve Crack Defects in Investment Casting of CN7M Material

Raw material316 stainless steelFerrosiliconElectrolytic manganeseMicrocarbon ferrochromeNickel plateFerromolybdenumElectrolytic copperTotal
Weight/kg49510520623220321000

In view of the above analysis results, our company changed the raw materials used in smelting during production, changed the purchased bar materials into various intermediate alloys for batching, and strictly controlled the content of Sn. See Table 1 for smelting proportioning.

NumberCSiMnPSCrNiMoCuAlSnAsPbSbFe
10.024 20.860.880.016 90.001 119.4728.032.173.330.018 10.057 60.002 10.001 8<0.002Bal.
20.031 30.790.910.017 70.001 219.6828.162.153.290.015 60.051 30.001 90.001 7<0.002Bal.
30.028 30.830.900.017 20.001 119.7128.222.153.270.016 70.055 30.001 90.001 8<0.002Bal.

After using the above smelting raw materials for production, through chemical analysis and detection, as shown in Table 2, the content of Sn element after smelting is about 0.005%, which is reduced to about 1/10 of that before the change, and the crack defect of the product is well solved. In addition to the change of smelting material and proportion, other parts are produced according to the original investment casting process, and there are no cracks in the investment castings, as shown in the figure.

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