This study addresses the recurring issue of shrinkage porosity in ZL205A aluminum alloy cylinder castings produced through conventional sand casting. Through systematic analysis of gating design, riser efficiency, and solidification characteristics, optimized solutions were developed to eliminate casting defects while maintaining process feasibility for mass production.

Initial Casting Process and Defect Manifestation
The cylindrical component (Ø600×700mm) with four internal T-ribs exhibited severe shrinkage porosity in preliminary trials. The original bottom-gating system featured:
| Component | Quantity | Cross-section (cm²) |
|---|---|---|
| Sprue | 1 | 7.0 |
| Runner | 1 | 8.4 |
| Gates | 4 | 14.0 |
The area ratio followed:
$$ \sum F_{sprue} : \sum F_{runner} : \sum F_{gate} = 1 : 1.2 : 1.7 $$
X-ray inspection revealed defect distribution patterns:
| Zone | Max Defect Length (mm) | Frequency |
|---|---|---|
| I | 60 | 4 |
| II | 40 | 4 |
| III | 75 | 4 |
| IV | 30 | 8 |
Root Cause Analysis of Casting Defects
Three primary factors contributed to shrinkage porosity formation:
1. Inverse Thermal Gradient: Bottom-gating created unfavorable temperature distribution:
$$ T_{upper} < T_{lower} $$
Resulting in upward solidification conflicting with gravity feeding.
2. Material Characteristics: ZL205A’s wide freezing range (544-633°C) promotes mushy zone formation:
$$ \frac{dT}{dt} = \alpha \nabla^2 T $$
Where α represents thermal diffusivity (≈ 5.6×10⁻⁵ m²/s for ZL205A).
3. Inadequate Feeding: Riser efficiency (η) calculations revealed insufficient compensation:
$$ \eta = \frac{V_{feed}}{V_{shrinkage}} \times 100\% < 68\% $$
Process Optimization Strategy
The redesigned feeding system achieved directional solidification through:
| Modification | Parameter Change | Effect |
|---|---|---|
| Sprue quantity | 1 → 2 | Reduced pouring time by 40% |
| Gate count | 4 → 8 | Improved temperature uniformity |
| Riser configuration | 4 top → 12 total | Increased feeding efficiency to 82% |
The optimized thermal gradient followed:
$$ \frac{\partial T}{\partial z} = 2.8^{\circ}C/cm \quad (z\text{-axis: bottom→top}) $$
Chvorinov’s Rule verification ensured proper riser sizing:
$$ t_{casting} = B\left(\frac{V}{A}\right)^n $$
Where B=3.2 (sand mold constant) and n=1.24 for ZL205A.
Validation and Production Implementation
Modified process parameters eliminated shrinkage porosity defects:
| Quality Metric | Initial | Optimized |
|---|---|---|
| X-ray defect density | 12 defects/m² | 0.8 defects/m² |
| Surface porosity area | 7.2% | <0.5% |
| Yield strength | 310 MPa | 345 MPa |
The successful resolution of casting defects demonstrates that systematic analysis of solidification dynamics combined with gating/riser optimization can effectively mitigate shrinkage porosity in complex aluminum castings. This approach provides a methodological framework for addressing similar casting defect challenges in heavy-section components.
