In the production of high manganese steel casting components, such as railway frogs, ensuring internal quality is critical due to their operation under heavy load and high-speed conditions. These high manganese steel casting parts must be free from shrinkage defects to maintain safety and durability. This article addresses a localized shrinkage defect observed in a specific high manganese steel casting frog, analyzing the root causes and presenting effective improvement strategies. Through detailed examination of riser design, feeding distance, and feeding channels, we implemented modifications that eliminated the defects, resulting in high-quality high manganese steel casting products.
The high manganese steel casting process involves significant volumetric shrinkage during solidification, which can lead to defects if not properly managed. In this case, the defect was identified in the toe end section of the frog, where the structure includes complex geometries like transverse ribs and risers. Initial inspections revealed shrinkage cavities in the rail top working surface, necessitating a thorough investigation. Our analysis focused on three key aspects: riser design adequacy, effective feeding distance, and the integrity of feeding channels. By applying principles of solidification theory, we developed solutions that enhanced the high manganese steel casting quality.

To begin, the high manganese steel casting structure of the frog features an open-bottom box design with integrated components like spacer irons and fishplates. The rail top and wall thicknesses are 34.9 mm and 25.4 mm, respectively, and the toe end has a thickened section due to structural and riser additions. This complexity increases the risk of shrinkage in high manganese steel casting, as the localized thick sections solidify later than surrounding areas. The original casting process used an open gating system with insulating risers and external chills, but this proved insufficient for preventing defects in the high manganese steel casting.
The primary cause of the shrinkage defect in this high manganese steel casting was inadequate riser design. The initial open riser had a modulus calculated as $$ M_{riser} = 1.2 \times M_{casting} $$ where \( M_{casting} = 3.0 \, \text{cm} \), giving \( M_{riser} = 3.6 \, \text{cm} \). However, the high volumetric shrinkage of high manganese steel casting, with a shrinkage rate \( \varepsilon = 8.5\% \), required a riser capable of feeding a larger mass. Based on casting manuals, the maximum feedable mass \( G \) for this riser was 56.8 kg, but the actual mass needing feeding \( G’ \) was 75 kg. Since \( G < G’ \), the riser could not provide sufficient feed metal, leading to shrinkage in the high manganese steel casting. The table below summarizes the riser parameters:
| Parameter | Original Value | Required Value |
|---|---|---|
| Riser Modulus (cm) | 3.6 | 4.32 |
| Feedable Mass (kg) | 56.8 | 75 |
| Shrinkage Rate (%) | 8.5 | 8.5 |
Another critical factor in high manganese steel casting is the effective feeding distance of the riser. For plate-like sections where the width-to-thickness ratio exceeds 5:1, the feeding distance \( L \) is given by \( L = 2\delta \), where \( \delta \) is the section thickness. In this high manganese steel casting, \( \delta = 40 \, \text{mm} \), so \( L = 80 \, \text{mm} \). However, the actual distance requiring feeding \( L’ \) was 150 mm, resulting in \( L < L’ \). This insufficient feeding distance exacerbated shrinkage defects in the high manganese steel casting, as the riser could not reach the entire solidifying region. The formula for feeding distance can be extended with chills to \( L = 2\delta + 2.5\delta \), which we applied in improvements.
The feeding channel in the high manganese steel casting also posed a problem. The narrowest part of the channel was thinner than the rail top working surface, causing it to solidify first and block feed metal flow. This interruption in feeding during the solidification of high manganese steel casting resulted in shrinkage cavities. To address this, we revised the design to ensure a gradual increase in channel thickness toward the riser, maintaining a feeding taper angle. This principle is rooted in directional solidification theory, where the feeding path must remain open until the final stages of high manganese steel casting solidification.
Our improvements for the high manganese steel casting involved three key changes. First, we replaced the open riser with an insulating exothermic riser, increasing the modulus to \( M_{riser} = 4.32 \, \text{cm} \). This enhanced the feeding capacity for the high manganese steel casting, as exothermic risers provide better heat retention and higher feeding efficiency. The new riser modulus was calculated based on the shrinkage rate and required feed mass, ensuring \( G \geq G’ \). Second, we incorporated external chills at the rail top working surface to create an artificial end zone, extending the feeding distance to \( L = 180 \, \text{mm} \), which exceeds \( L’ = 150 \, \text{mm} \). This is expressed as:
$$ L = 2\delta + 2.5\delta = 2 \times 40 + 2.5 \times 40 = 180 \, \text{mm} $$
The chills accelerate cooling in specific areas, promoting directional solidification in high manganese steel casting. Third, we increased the riser pad size to widen the feeding channel, ensuring a continuous feed metal flow. The table below compares the original and improved parameters:
| Aspect | Original Design | Improved Design |
|---|---|---|
| Riser Type | Open Riser | Exothermic Insulating Riser |
| Riser Modulus (cm) | 3.6 | 4.32 |
| Feeding Distance (mm) | 80 | 180 |
| Feeding Channel Design | Narrow, Constricted | Widened with Taper |
After implementing these changes in the high manganese steel casting process, we conducted trial productions and performed macro-section inspections. The results showed complete elimination of shrinkage defects in the rail top working surface and riser pad areas. The high manganese steel casting exhibited dense, defect-free microstructures, meeting all technical specifications. Multiple production batches confirmed the consistency of these improvements, validating our approach to enhancing high manganese steel casting quality.
In conclusion, the shrinkage defect in this high manganese steel casting was successfully resolved by optimizing riser design, extending feeding distance with chills, and ensuring open feeding channels. These measures align with solidification principles specific to high manganese steel casting, such as managing high volumetric shrinkage and promoting directional solidification. The effectiveness of these strategies underscores the importance of detailed process analysis in high manganese steel casting, leading to reliable components for demanding applications. Future work could explore further refinements in high manganese steel casting techniques to prevent similar defects.
