1. Introduction
In the manufacturing of large engine cylinder block, the post-casting processes, particularly automated grinding, play a pivotal role in ensuring dimensional accuracy and surface quality. However, due to the structural complexity and diverse specifications of cylinder block, achieving consistent results in automated grinding has been a persistent challenge. This article details our systematic approach to mitigating grinding-induced damage during the automation of cylinder block finishing, focusing on five critical dimensions: Human, Machine, Material, Method, and Measurement (H4M).

2. Current Challenges in Automated Grinding of Cylinder Block
Automated grinding systems for cylinder block often face high defect rates compared to manual processes. During initial trials, 510 cylinder block were processed, with 45 units damaged—a defect rate of 8.82%, far exceeding the manual grinding average of 0.13%. Common defects included localized over-grinding, tool jamming, and positional deviations (Figure 1).
Table 1: Defect Types and Frequencies in Automated Grinding
Defect Type | Frequency (%) | Root Cause |
---|---|---|
Localized Over-Grinding | 4.2% | Incorrect toolpath or laser compensation |
Tool Jamming | 2.8% | Excessive residual burr thickness |
Positional Deviation | 1.8% | Platform displacement during loading |
3. Root Cause Analysis Using the H4M Framework
3.1 Human Factors
Operators often misselected grinding programs due to subtle differences between cylinder block variants within the same series. For instance, a 0.5 mm variation in casting geometry could trigger mismatched toolpaths.
Table 2: Human-Related Risks and Mitigations
Risk | Mitigation Strategy |
---|---|
Program selection errors | Implement suffix-based input verification |
Inconsistent operator training | Standardize training modules for HMI navigation |
3.2 Machine Factors
The integration of loading and grinding platforms caused displacement due to cylinder block impact during loading. A 5 mm amplitude shift was observed under maximum load. Additionally, worn tooling fixtures exacerbated positional inaccuracies.
Equation 1: Impact Force During Loading
F=m⋅aF=m⋅a
Where FF = impact force, mm = cylinder block mass, aa = deceleration during placement.
Table 3: Machine-Related Improvements
Improvement | Outcome |
---|---|
Separate loading/grinding platforms | Reduced platform displacement by 80% |
Speed-adjustable crane system | Minimized impact force during placement |
3.3 Material Factors
Excessive residual burrs (>10 mm thickness) from rough grinding increased grinding resistance, leading to tool jamming.
Table 4: Material Standards for Burr Control
Parameter | Threshold | Measurement Method |
---|---|---|
Burr height | ≤10 mm | Laser profilometry |
Burr thickness | ≤8 mm | Cross-sectional sampling |
3.4 Method Factors
Toolpaths occasionally overlapped with machining datum points, causing unintended material removal. Structural design changes in cylinder block also disrupted preprogrammed paths.
Table 5: Methodological Enhancements
Action | Result |
---|---|
Exclude machining datums | Eliminated 95% of datum-related over-grinding |
Design change notification | Reduced path reprogramming time by 40% |
3.5 Measurement Factors
Single-point laser compensation failed to account for surface variations in sand-cast cylinder block. Multi-point averaging improved accuracy.
Equation 2: Multi-Point Compensation
Davg=1n∑i=1nDiDavg=n1i=1∑nDi
Where DavgDavg = compensated depth, DiDi = depth at point ii.
Table 6: Laser Measurement Optimization
Parameter | Before | After |
---|---|---|
Measurement points | 1 | 3 |
Compensation accuracy | ±1.5 mm | ±0.5 mm |
4. Implementation and Results
After implementing H4M-based solutions, the defect rate for cylinder block grinding dropped to 0.76%. Key outcomes include:
- Human: 100% program selection accuracy via suffix verification.
- Machine: Platform displacement reduced to ≤1 mm.
- Material: Burr-related defects decreased by 70%.
- Method: Zero datum-point grinding errors.
- Measurement: Laser compensation accuracy improved by 67%.
Table 7: Post-Improvement Performance Metrics
Metric | Initial Value | Final Value | Improvement |
---|---|---|---|
Defect rate | 8.82% | 0.76% | 91.4% |
Platform displacement | 5 mm | 1 mm | 80% |
Burr-related jamming | 2.8% | 0.8% | 71.4% |
5. Conclusion
By systematically addressing H4M factors, we achieved a 91.4% reduction in grinding defects for large engine cylinder block. Future work will focus on AI-driven toolpath optimization and real-time adaptive compensation to further enhance the robustness of automated grinding systems.