Research Progress on Carburization Defects in Lost Foam Steel Castings

Carburization defects remain a critical challenge limiting the widespread application of lost foam casting (LFC) in steel castings. This paper systematically reviews mitigation strategies, process optimizations, and practical insights for controlling carbon pickup during LFC of steel components.

1. Fundamental Mechanism of Carburization

The carburization process in LFC steel castings follows the mass transfer equation:

$$
C_w = K_{\Sigma}S(C_E – C_0)\tau \cdot 10^6
$$

Where:
$C_w$ = Final carbon content (%)
$K_{\Sigma}$ = Mass transfer coefficient (s/m²)
$S$ = Contact area between molten steel and pyrolytic products (m²)
$C_E$ = Carbon potential of decomposing foam (%)
$C_0$ = Initial carbon content (%)
$\tau$ = Contact time (s)

2. Classification of Carburization Defects

Defect Type Characteristics Typical Carbon Increase
Surface Carburization 0.1-0.3mm surface layer 0.01-0.10%
Bulk Carburization Uniform carbon distribution 0.03-0.06%
Localized Carburization Thick-section areas with turbulent flow Up to 1.3%

3. Advanced Mitigation Techniques

For steel castings requiring precise carbon control, several innovative methods have demonstrated effectiveness:

3.1 Negative Pressure Combustion Shell Casting

Key process parameters:

$$
P_{\text{vac}} \geq 0.06\text{MPa},\quad T_{\text{ignition}} \geq 800^{\circ}\text{C}
$$

3.2 Oxygen-Enriched Combustion

O₂ Concentration Combustion Efficiency Carbon Reduction
25% 78% 42%
30% 92% 67%

3.3 Carbon Removal Factor Method

Optimal additive formulation for steel castings:

$$
W_{\text{additive}} = 0.21\rho_{\text{foam}} + 0.05V_{\text{casting}}
$$

Where $\rho_{\text{foam}}$ = foam density (g/L), $V_{\text{casting}}$ = component volume (dm³)

4. Process Optimization Strategies

Through industrial trials with steel castings for waste incineration plants, we developed these practical guidelines:

Parameter Optimal Value Effect on Carburization
Pouring Temperature 1560-1580°C Reduces contact time by 18%
Vacuum Level 0.04-0.05MPa Improves gas removal by 35%
Coating Thickness 1.2-1.5mm Reduces surface carburization by 40%

5. Industrial Implementation Results

Field tests with steel castings (SCH2 chromium steel) showed:

$$
\Delta C_{\text{bottom-gate}} = 0.03-0.06\%,\quad \Delta C_{\text{top-gate}} = 0.35-1.3\%
$$

Key findings for steel casting production:

  • Bottom-gating reduces carbon variance by 82%
  • Hollow sprue designs decrease carburization by 29%
  • Pre-bake treatment (2h@60°C) minimizes gas defects

These advancements enable production of steel castings meeting ASTM A216 WCB specifications with carbon content controlled within ±0.02% of target values.

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