Causes of shrinkage defects in castings
The basic cause of concentrated shrinkage defects in castings is that the liquid shrinkage and solidification shrinkage of the alloy […]
The basic cause of concentrated shrinkage defects in castings is that the liquid shrinkage and solidification shrinkage of the alloy […]
The multi-element alloy additive is designed according to the research results at home and abroad on the influence of Alloying
The coupler body of type 17 coupler is a complex medium and small steel casting with the overall size of
In the process of gray cast iron cutting experiment, the measurement cycle is 20 s, the cutting length of the
During the trial production of coupler steel castings, the process scheme is continuously optimized and the casting quality is continuously
The coupler knuckle is connected with the coupler body through the coupler knuckle pin. During the operation of the vehicle
Visual inspection is not only the first step in the delivery inspection of cast steel joints, but also an essential
Due to the existence of graphite in common gray cast iron, and the tensile strength of graphite is almost zero,
After the production line of type 16 knuckle product is arranged and runs well, the trial production of the product
The improved process scheme is adopted for the hook body steel casting to simulate the mold filling and solidification process.
The hook tongue adopts the improved sand casting process scheme to simulate the mold filling and solidification process. The pouring
There are 14 sand cores in the motor shell in total, and the assembly of sand cores is shown in
In terms of detection methods, GB7233-09 focuses on the near-field area of ultrasonic flaw detection, and adds a near-field resolution
Figures 1 to 3 show the simulation analysis results of the casting solidification process of the hook tongue. Figure 1
Figure 1 to figure 4 show the simulation analysis results of the hook tongue filling process. Figure 1 shows the
Firstly, cast the steel castings of the coupler according to the original casting process design. The main problems exposed are:
Type 16 coupler knuckle is a complex small steel casting. The overall size of the steel casting of coupler knuckle
By adding different content of copper and different ratio of copper and chromium, the mechanical properties and cutting properties of
Figure 1 shows the temperature distribution results of the hook body 5 s after it starts to solidify. The solidification
Figures 1 to 4 show the simulation analysis results of the mold filling process of hook steel castings. Figure 1
The total number of cracks in the motor shell produced by furan resin sand casting process is about 70, while
According to the previous casting simulation results, it is found that the process riser of the steel casting plant is
The sand inclusion casting defects of steel castings are relatively serious, because the proportion of product scrapping caused by sand
The coupler body of type 17 coupler is a complex medium and small steel casting with the overall size of
The mechanical properties and machinability of gray cast iron samples for engine cylinder block were tested, and the microstructure of
① Analysis on the original pouring system of motor shell See Fig. 1 for the original pouring system of motor
Before the proportion of molding sand is proposed, the basic range of molding sand properties should be determined according to
The orthogonal experiment will be designed, the riser height is set as the independent variable, and other process parameters remain
Casting sand inclusion defects are directly related to production process, mold, sand mixing, molding, core making, lower core box, pouring
Figure 1 shows the simulation results of temperature field at each time during solidification of mud pump body in sand